JP2738281B2 - Hot rolling method of stainless steel slab - Google Patents

Hot rolling method of stainless steel slab

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Publication number
JP2738281B2
JP2738281B2 JP32484293A JP32484293A JP2738281B2 JP 2738281 B2 JP2738281 B2 JP 2738281B2 JP 32484293 A JP32484293 A JP 32484293A JP 32484293 A JP32484293 A JP 32484293A JP 2738281 B2 JP2738281 B2 JP 2738281B2
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JP
Japan
Prior art keywords
slab
scale
temperature
furnace
hot
Prior art date
Legal status (The legal status is an assumption and is not a legal conclusion. Google has not performed a legal analysis and makes no representation as to the accuracy of the status listed.)
Expired - Fee Related
Application number
JP32484293A
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Japanese (ja)
Other versions
JPH07178420A (en
Inventor
正宏 片平
俊暁 松浦
龍至 平井
Current Assignee (The listed assignees may be inaccurate. Google has not performed a legal analysis and makes no representation or warranty as to the accuracy of the list.)
JFE Engineering Corp
Original Assignee
Nippon Kokan Ltd
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Publication date
Application filed by Nippon Kokan Ltd filed Critical Nippon Kokan Ltd
Priority to JP32484293A priority Critical patent/JP2738281B2/en
Publication of JPH07178420A publication Critical patent/JPH07178420A/en
Application granted granted Critical
Publication of JP2738281B2 publication Critical patent/JP2738281B2/en
Anticipated expiration legal-status Critical
Expired - Fee Related legal-status Critical Current

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  • Metal Rolling (AREA)
  • Heat Treatment Of Steel (AREA)

Description

【発明の詳細な説明】DETAILED DESCRIPTION OF THE INVENTION

【0001】[0001]

【産業上の利用分野】本発明は、熱間圧延時にスケール
疵を生じない表面性状に優れたステンレス鋼スラブの熱
間圧延方法に関する。
BACKGROUND OF THE INVENTION 1. Field of the Invention The present invention relates to a method for hot rolling a stainless steel slab which does not cause scale flaws during hot rolling and has excellent surface properties.

【0002】[0002]

【従来の技術】ステンレス鋼の熱間圧延では、スラブ加
熱時に生成するスケールが原因で、スケール疵が生じ表
面性状を著しく悪化させている。従来からスケール疵の
防止対策として種々の提案がなされている。
2. Description of the Related Art In hot rolling of stainless steel, scale flaws are generated due to scale generated at the time of slab heating, and surface properties are remarkably deteriorated. Conventionally, various proposals have been made as measures for preventing scale flaws.

【0003】第1にスケールの発生は不可避とする考え
かたによるスケール疵の防止対策があげられる。第2に
スケールの発生そのものを抑制するスケール疵の防止対
策があげられる。これらの防止対策のなかでも比較的実
操業において効果的と思われるものに、特開昭61−1
11703号公報、特開昭62−13527号公報、並
びに特開平4−138803号公報をあげることができ
る。これらの提案は、いずれもスラブ表面におけるスケ
ール発生を抑制する方法として、スラブを比較的低温域
で短時間だけ加熱することを骨子としている。
First, there is a measure for preventing scale flaws by considering that generation of scale is inevitable. Second, there is a measure for preventing scale flaws that suppresses the generation of scale itself. Among these preventive measures, one which is considered to be relatively effective in actual operation is disclosed in JP-A-61-1.
JP-A-11703, JP-A-62-13527 and JP-A-4-138803 can be mentioned. In any of these proposals, as a method of suppressing scale generation on the slab surface, the main point is to heat the slab in a relatively low temperature range for a short time.

【0004】[0004]

【発明が解決しようとする課題】しかしながら、従来の
方法においては、低温加熱することにより変形抵抗が増
し、圧延能率が低下する。さらに薄物材では圧延温度が
低下し耳割れが発生すると共に、製造可能寸法が制限さ
れてしまう。このため、上記の従来技術では生産性の確
保と表面品質の改善という両者を満足させることが困難
であった。
However, in the conventional method, the deformation resistance is increased by heating at a low temperature, and the rolling efficiency is reduced. Further, in the case of a thin material, the rolling temperature is lowered to cause ear cracks, and the manufacturable dimensions are limited. For this reason, it is difficult for the above-mentioned conventional technology to satisfy both of securing the productivity and improving the surface quality.

【0005】本発明は、熱間圧延時の脱スケール性を改
善し、スケール疵発生のない表面性状に優れた製品を得
ることができるステンレス鋼スラブの熱間圧延方法を提
供することを目的とする。
An object of the present invention is to provide a method for hot rolling a stainless steel slab which can improve descalability during hot rolling and can provide a product having excellent surface properties without scale flaws. I do.

【0006】[0006]

【課題を解決するための手段】従来、ステンレス鋼の表
面疵防止において、スラブ加熱時にスケールが生じて
も、デスケールが完全に行われれば表面疵は発生しない
という観点からの検討は行われていない。そこで、デス
ケールの容易さとスケールの性状について、発明者らは
詳細に検討を行った。
Means for Solving the Problems Conventionally, in the prevention of surface flaws of stainless steel, no study has been made from the viewpoint that no surface flaws will be generated if descale is performed completely even if scales are generated during slab heating. . Then, the inventors examined in detail the ease of descale and the properties of the scale.

【0007】その結果、スケールのデスケール性はスラ
ブ表層に形成されるCr酸化層中のメタル混在量に依存
し、その量はスケールの生成する温度によるとの知見を
得た。すなわち、高温で形成されるCr酸化層は、メタ
ル混在となるため、メタルとの密着性がよく脱スケール
性が悪いが、低温で形成されるCr酸化層はメタルをほ
とんど含まず緻密なスケールとなるため、脱スケール性
が良好である。
As a result, it has been found that the descalability of the scale depends on the amount of metal contained in the Cr oxide layer formed on the surface layer of the slab, and that the amount depends on the temperature at which the scale is formed. In other words, the Cr oxide layer formed at a high temperature contains a mixture of metals, and therefore has good adhesion to metal and poor descalability, but the Cr oxide layer formed at a low temperature contains little metal and has a dense scale. Therefore, descalability is good.

【0008】本発明に係るステンレス鋼スラブの熱間圧
延方法は、ステンレス鋼スラブを1000℃乃至110
0℃の温度範囲で1時間乃至3時間にわたり均熱保持
し、さらに前記スラブを1150乃至1250℃の温度
範囲で2時間以上にわたり均熱保持した後に、熱間圧延
することを特徴とする。
[0008] In the hot rolling method for a stainless steel slab according to the present invention, the stainless steel slab is heated to 1000 ° C to 110 ° C.
The slab is soaked for 1 to 3 hours in a temperature range of 0 ° C., and the slab is soaked for 2 hours or more in a temperature range of 1150 to 1250 ° C., and then hot-rolled.

【0009】[0009]

【作用】本発明に係るステンレス鋼スラブの熱間圧延方
法においては、スラブ加熱の第1段階(低温段階)でま
ず緻密なスケールをスラブ表面に生成させる。このスケ
ールはメタルを含まないため、表面疵を防止するために
十分なデスケール性が確保される。その後、圧延性の確
保を目的にスラブ加熱を行うが、それにより生じるスケ
ールは、脱スケール性に優れるスケールを基地として成
長することになるため、熱間圧延工程でのデスケール作
業で表面疵を防止するに十分な脱スケール性を示す。
In the hot rolling method for a stainless steel slab according to the present invention, first, a dense scale is formed on the slab surface in the first stage (low temperature stage) of slab heating. Since this scale does not contain metal, sufficient descaling property is secured to prevent surface flaws. After that, slab heating is performed for the purpose of ensuring rollability, but the resulting scale grows on the basis of scale with excellent descaling properties, so surface defects are prevented by descale work in the hot rolling process Shows sufficient descaling property.

【0010】すなわち、低温/短時間加熱がスケール防
止のため有効であることは周知であるが、本発明の特許
性は圧延性を確保するために行うスラブ加熱で生じるス
ケールの生地として、低温加熱で生成する緻密なスケー
ル層をいわゆる保護皮膜として採用すればよいというこ
とを見いだした点にある。
That is, although it is well known that low-temperature / short-time heating is effective for preventing scale, the patentability of the present invention is that low-temperature heating is used as a scale material produced by slab heating performed to ensure rollability. It has been found that the fine scale layer generated by the above method may be used as a so-called protective film.

【0011】次に、第1段階及び第2段階の加熱条件を
限定した理由について述べる。1段目の加熱により緻密
なスケール層を生成させるためには、1000℃未満で
はスケール生成に長時間を有し、1100℃を越える温
度ではメタル混在スケールが生成して脱スケール性が低
下するため、1000〜1100℃に限定した。また、
均熱時間はスケール層生成のためには1時間以上必要で
あり、長時間加熱は操業上のロスが大きいため、1〜3
時間に限定した。
Next, the reason why the heating conditions in the first and second stages are limited will be described. In order to form a dense scale layer by heating at the first stage, if the temperature is lower than 1000 ° C., it takes a long time to generate the scale. , 1000-1100 ° C. Also,
The soaking time is 1 hour or more for the formation of the scale layer, and long-time heating causes a large loss in operation.
Limited to time.

【0012】最終のスラブ加熱条件は、圧延性の観点か
ら高温加熱が望ましいが、1250℃を越えて加熱する
とスケール/メタル界面の反応が進み、新たにメタル混
在スケールが生成するため、上限温度を1250℃とし
た。一方、最終のスラブ加熱温度が1150℃未満であ
ると添加元素がその後の熱処理に必要な十分な固溶状態
にならないため、下限温度を1150℃とした。
As the final slab heating conditions, high-temperature heating is desirable from the viewpoint of rollability. However, if the temperature exceeds 1250 ° C., the reaction at the scale / metal interface proceeds, and a metal-mixed scale is newly formed. It was 1250 ° C. On the other hand, if the final slab heating temperature is lower than 1150 ° C., the additional element does not have a sufficient solid solution state required for the subsequent heat treatment, so the lower limit temperature was set to 1150 ° C.

【0013】なお、均熱時間は、スラブを均一に加熱す
るために2時間以上が必要である。ちなみに本発明にお
けるスラブ加熱後の熱間圧延は、通常操業において実施
しているものでよく、とくに特殊な工程を必要としな
い。
The soaking time requires at least 2 hours in order to uniformly heat the slab. Incidentally, the hot rolling after slab heating in the present invention may be carried out in a normal operation, and does not require any special process.

【0014】[0014]

【実施例】以下、本発明の種々の実施例について表1を
参照しながら比較例と対比して説明する。JIS規格S
US304、SUS430並びにSUS329J3Lの
3鋼種を供試材に用いて、加熱条件を種々変えてスラブ
を加熱した後に熱間圧延し、そのときのスケール疵の発
生状況を調べた。各加熱条件ごとにスラブを100枚ず
つ圧延した。圧延後、スラブを溶体化熱処理し、酸洗
し、その表面を目視にて観察した。その結果はスケール
疵発生率によって評価判定した。ここで「スケール疵発
生率」とは100枚のうち何枚のスラブ表面にスケール
疵が生じたかを百分率(%)で表した指数をいう。
Hereinafter, various examples of the present invention will be described with reference to Table 1 in comparison with comparative examples. JIS standard S
Using three steel types of US304, SUS430 and SUS329J3L as test materials, the slab was heated under various heating conditions and then hot-rolled, and the occurrence of scale flaws at that time was examined. 100 slabs were rolled for each heating condition. After rolling, the slab was subjected to solution heat treatment, pickling, and the surface was visually observed. The results were evaluated and judged based on the scale flaw occurrence rate. Here, the “scale flaw occurrence rate” refers to an index expressing the number of scale flaws on the slab surface out of 100 pieces as a percentage (%).

【0015】表1には一例として実施例1〜8及び比較
例1〜7を示す。実施例1〜8は本発明方法に含まれる
条件下でそれぞれ熱間圧延したスラブ表面を調べた結果
にあたる。一方、比較例1〜7は従来方法の条件下およ
び本発明方法の条件から外れる条件下でそれぞれ熱間圧
延したスラブ表面を調べた結果にあたる。以下、それぞ
れの条件および結果について説明する。 [実施例1]厚さ300mmのSUS304スラブを均熱
炉内で約1000℃の温度で約1時間にわたり均熱保持
した。さらに、これを均熱炉内で約1150℃の温度で
約5時間にわたり均熱保持した。均熱炉内は酸素ガスを
含むガス雰囲気(高炉ガスを炉内に導入)に調整されて
いる。次いで、炉内からスラブを搬出し、圧延ラインに
てこれを熱間圧延し、最終的に50mmの製品に仕上げ
た。
Table 1 shows Examples 1 to 8 and Comparative Examples 1 to 7 as examples. Examples 1 to 8 correspond to the results of examining the slab surface which was hot-rolled under the conditions included in the method of the present invention. On the other hand, Comparative Examples 1 to 7 correspond to the results of examining the slab surface which was hot-rolled under conditions of the conventional method and conditions deviating from the conditions of the method of the present invention, respectively. Hereinafter, each condition and result will be described. Example 1 A SUS304 slab having a thickness of 300 mm was soaked in a soaking furnace at a temperature of about 1000 ° C. for about 1 hour. Further, it was kept in a soaking furnace at a temperature of about 1150 ° C. for about 5 hours. The inside of the soaking furnace is adjusted to a gas atmosphere containing oxygen gas (blast furnace gas is introduced into the furnace). Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0016】スラブ100枚について調べたところスケ
ール疵発生率は1%であった。 [実施例2]厚さ300mmのSUS304スラブを均熱
炉内で約1000℃の温度で約3時間にわたり均熱保持
した。さらに、これを均熱炉内で約1250℃の温度で
約5時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に50mmの製品に仕上げた。
When 100 slabs were examined, the scale flaw occurrence rate was 1%. Example 2 A SUS304 slab having a thickness of 300 mm was kept in a soaking furnace at a temperature of about 1000 ° C. for about 3 hours. Further, it was kept in a soaking furnace at a temperature of about 1250 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0017】スラブ100枚について調べたところスケ
ール疵発生率は3%であった。 [実施例3]厚さ300mmのSUS304スラブを均熱
炉内で約1050℃の温度で約1時間にわたり均熱保持
した。さらに、これを均熱炉内で約1150℃の温度で
約5時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に50mmの製品に仕上げた。
Examination of 100 slabs revealed that the scale flaw occurrence rate was 3%. Example 3 A SUS304 slab having a thickness of 300 mm was soaked in a soaking furnace at a temperature of about 1050 ° C. for about 1 hour. Further, it was kept in a soaking furnace at a temperature of about 1150 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0018】スラブ100枚について調べたところスケ
ール疵発生率は1%であった。 [実施例4]厚さ300mmのSUS304スラブを均熱
炉内で約1050℃の温度で約3時間にわたり均熱保持
した。さらに、これを均熱炉内で約1250℃の温度で
約5時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に50mmの製品に仕上げた。
When 100 slabs were examined, the scale flaw occurrence rate was 1%. Example 4 A SUS304 slab having a thickness of 300 mm was kept in a soaking furnace at a temperature of about 1050 ° C. for about 3 hours. Further, it was kept in a soaking furnace at a temperature of about 1250 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0019】スラブ100枚について調べたところスケ
ール疵発生率は3%であった。 [実施例5]厚さ300mmのSUS304スラブを均熱
炉内で約1100℃の温度で約1時間にわたり均熱保持
した。さらに、これを均熱炉内で約1200℃の温度で
約5時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に50mmの製品に仕上げた。
When 100 slabs were examined, the scale flaw generation rate was 3%. Example 5 A SUS304 slab having a thickness of 300 mm was soaked in a soaking furnace at a temperature of about 1100 ° C. for about 1 hour. Further, this was kept in a soaking furnace at a temperature of about 1200 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0020】スラブ100枚について調べたところスケ
ール疵発生率は2%であった。 [実施例6]厚さ300mmのSUS304スラブを均熱
炉内で約1100℃の温度で約3時間にわたり均熱保持
した。さらに、これを均熱炉内で約1250℃の温度で
約5時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に50mmの製品に仕上げた。
When 100 slabs were examined, the scale flaw occurrence rate was 2%. Example 6 A SUS304 slab having a thickness of 300 mm was soaked in a soaking furnace at a temperature of about 1100 ° C. for about 3 hours. Further, it was kept in a soaking furnace at a temperature of about 1250 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0021】スラブ100枚について調べたところスケ
ール疵発生率は4%であった。 [実施例7]厚さ150mmのSUS430スラブを均熱
炉内で約1050℃の温度で約2時間にわたり均熱保持
した。さらに、これを均熱炉内で約1200℃の温度で
約3時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に12mmの製品に仕上げた。
Examination of 100 slabs revealed that the scale flaw occurrence rate was 4%. Example 7 A SUS430 slab having a thickness of 150 mm was kept in a soaking furnace at a temperature of about 1050 ° C. for about 2 hours. Further, it was kept in a soaking furnace at a temperature of about 1200 ° C. for about 3 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 12 mm product.

【0022】スラブ100枚について調べたところスケ
ール疵発生率は1%であった。 [実施例8]厚さ150mmのSUS329J3Lスラブ
を均熱炉内で約1050℃の温度で約2時間にわたり均
熱保持した。さらに、これを均熱炉内で約1200℃の
温度で約3時間にわたり均熱保持した。次いで、炉内か
らスラブを搬出し、圧延ラインにてこれを熱間圧延し、
最終的に12mmの製品に仕上げた。
When 100 slabs were examined, the scale flaw occurrence rate was 1%. Example 8 A SUS329J3L slab having a thickness of 150 mm was kept in a soaking furnace at a temperature of about 1050 ° C. for about 2 hours. Further, it was kept in a soaking furnace at a temperature of about 1200 ° C. for about 3 hours. Next, the slab is unloaded from the furnace and hot-rolled on a rolling line.
Finally, the product was finished to 12 mm.

【0023】スラブ100枚について調べたところスケ
ール疵発生率は1%であった。 [比較例1]厚さ300mmのSUS304スラブを均熱
炉内で約1150℃の温度で約5時間にわたり均熱保持
した。次いで、炉内からスラブを搬出し、圧延ラインに
てこれを熱間圧延し、最終的に50mmの製品に仕上げ
た。
When 100 slabs were examined, the scale flaw occurrence rate was 1%. Comparative Example 1 A SUS304 slab having a thickness of 300 mm was kept in a soaking furnace at a temperature of about 1150 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0024】スラブ100枚について調べたところスケ
ール疵発生率は15%であった。 [比較例2]厚さ300mmのSUS304スラブを均熱
炉内で約1250℃の温度で約5時間にわたり均熱保持
した。次いで、炉内からスラブを搬出し、圧延ラインに
てこれを熱間圧延し、最終的に50mmの製品に仕上げ
た。
When 100 slabs were examined, the scale flaw occurrence rate was 15%. Comparative Example 2 A SUS304 slab having a thickness of 300 mm was held in a soaking furnace at a temperature of about 1250 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0025】スラブ100枚について調べたところスケ
ール疵発生率は16%であった。 [比較例3]厚さ300mmのSUS304スラブを均熱
炉内で約1050℃の温度で約30分間にわたり均熱保
持した。さらに、これを均熱炉内で約1150℃の温度
で約5時間にわたり均熱保持した。次いで、炉内からス
ラブを搬出し、圧延ラインにてこれを熱間圧延し、最終
的に50mmの製品に仕上げた。
Examination of 100 slabs revealed that the scale flaw generation rate was 16%. Comparative Example 3 A SUS304 slab having a thickness of 300 mm was soaked in a soaking furnace at a temperature of about 1050 ° C. for about 30 minutes. Further, it was kept in a soaking furnace at a temperature of about 1150 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0026】スラブ100枚について調べたところスケ
ール疵発生率は14%であった。 [比較例4]厚さ300mmのSUS304スラブを均熱
炉内で約1150℃の温度で約2時間にわたり均熱保持
した。さらに、これを均熱炉内で約1250℃の温度で
約5時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に50mmの製品に仕上げた。
When 100 slabs were examined, the scale flaw occurrence rate was 14%. Comparative Example 4 A SUS304 slab having a thickness of 300 mm was kept in a soaking furnace at a temperature of about 1150 ° C. for about 2 hours. Further, it was kept in a soaking furnace at a temperature of about 1250 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0027】スラブ100枚について調べたところスケ
ール疵発生率は18%であった。 [比較例5]厚さ300mmのSUS304スラブを均熱
炉内で約1050℃の温度で約2時間にわたり均熱保持
した。さらに、これを均熱炉内で約1300℃の温度で
約5時間にわたり均熱保持した。次いで、炉内からスラ
ブを搬出し、圧延ラインにてこれを熱間圧延し、最終的
に50mmの製品に仕上げた。
When 100 slabs were examined, the scale flaw occurrence rate was 18%. Comparative Example 5 A SUS304 slab having a thickness of 300 mm was kept in a soaking furnace at a temperature of about 1050 ° C. for about 2 hours. Further, it was kept in a soaking furnace at a temperature of about 1300 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0028】スラブ100枚について調べたところスケ
ール疵発生率は23%であった。 [比較例6]厚さ300mmのSUS430スラブを均熱
炉内で約1150℃の温度で約5時間にわたり均熱保持
した。次いで、炉内からスラブを搬出し、圧延ラインに
てこれを熱間圧延し、最終的に50mmの製品に仕上げ
た。
When 100 slabs were examined, the scale flaw occurrence rate was 23%. Comparative Example 6 A SUS430 slab having a thickness of 300 mm was kept in a soaking furnace at a temperature of about 1150 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0029】スラブ100枚について調べたところスケ
ール疵発生率は30%であった。 [比較例7]厚さ300mmのSUS329J3Lスラブ
を均熱炉内で約1200℃の温度で約5時間にわたり均
熱保持した。次いで、炉内からスラブを搬出し、圧延ラ
インにてこれを熱間圧延し、最終的に50mmの製品に仕
上げた。
When 100 slabs were examined, the scale flaw occurrence rate was 30%. Comparative Example 7 A SUS329J3L slab having a thickness of 300 mm was kept in a soaking furnace at a temperature of about 1200 ° C. for about 5 hours. Next, the slab was unloaded from the furnace, and was hot-rolled in a rolling line to finally obtain a 50 mm product.

【0030】スラブ100枚について調べたところスケ
ール疵発生率は33%であった。上記の比較例1及び比
較例2(SUS304)の結果から明らかなように、低
温加熱(1000〜1100℃の第1段階加熱)するこ
となく、いきなり1150℃以上の温度域にスラブを加
熱するとスケール疵発生率は15〜16%にも達する。
これに対して実施例1〜6の結果から明らかなように、
第1段階及び第2段階において適正条件でスラブを加熱
すると、スケール疵発生率は1〜4%まで低減された。
When 100 slabs were examined, the scale flaw occurrence rate was 33%. As is clear from the results of Comparative Example 1 and Comparative Example 2 (SUS304), if the slab is heated to a temperature range of 1150 ° C. or more without heating at a low temperature (first stage heating at 1000 to 1100 ° C.), the scale becomes large. The flaw generation rate reaches as much as 15-16%.
On the other hand, as is clear from the results of Examples 1 to 6,
When the slab was heated under appropriate conditions in the first and second stages, the scale flaw occurrence rate was reduced to 1-4%.

【0031】また、比較例3(SUS304)の結果か
ら明らかなように、第1段階加熱保持時間が30分間と
短かすぎると、その後の第2段階加熱において適正条件
で加熱したとしてもスケール疵発生率は14%にも達す
る。これに対して実施例1〜6の結果から明らかなよう
に、第1段階及び第2段階において適正条件でスラブを
加熱すると、スケール疵発生率は1〜4%まで低減され
た。
Further, as is apparent from the results of Comparative Example 3 (SUS304), if the first-stage heating holding time is too short, that is, 30 minutes, even if heating is performed under appropriate conditions in the subsequent second-stage heating, scale flaws will occur. The incidence can be as high as 14%. On the other hand, as is clear from the results of Examples 1 to 6, when the slab was heated under appropriate conditions in the first and second stages, the scale flaw occurrence rate was reduced to 1 to 4%.

【0032】さらに、比較例4(SUS304)の結果
から明らかなように、第1段階加熱における温度が11
50℃と高くなりすぎると、その後の第2段階加熱にお
いて適正条件で加熱したとしてもスケール疵発生率は1
8%に増加する。これに対して実施例1〜6の結果から
明らかなように、第1段階及び第2段階において適正条
件でスラブを加熱すると、スケール疵発生率は1〜4%
まで低減された。
Further, as is apparent from the results of Comparative Example 4 (SUS304), the temperature in the first stage heating was 11
If the temperature is too high at 50 ° C., the scale flaw generation rate will be 1 even if heating is performed under appropriate conditions in the subsequent second stage heating.
Increase to 8%. On the other hand, as is clear from the results of Examples 1 to 6, when the slab is heated under appropriate conditions in the first stage and the second stage, the scale flaw generation rate becomes 1 to 4%
Reduced to

【0033】さらに、比較例5(SUS304)の結果
から明らかなように、第1段階加熱において適正条件で
加熱したとしても、その後の第2段階加熱における加熱
温度が高くなりすぎるとスケール疵発生率は23%に増
加する。これに対して実施例1〜6の結果から明らかな
ように、第1段階及び第2段階において適正条件でスラ
ブを加熱すると、スケール疵発生率は1〜4%まで低減
された。
Further, as is clear from the results of Comparative Example 5 (SUS304), even if the first stage heating was performed under appropriate conditions, if the heating temperature in the subsequent second stage heating was too high, the scale flaw generation rate was high. Increases to 23%. On the other hand, as is clear from the results of Examples 1 to 6, when the slab was heated under appropriate conditions in the first and second stages, the scale flaw occurrence rate was reduced to 1 to 4%.

【0034】さらに、比較例6(SUS430)の結果
から明らかなように、第1段階加熱することなく、いき
なり1150℃以上の温度域にスラブを加熱するとスケ
ール疵発生率は30%に増加する。これに対して実施例
7の結果から明らかなように、第1段階及び第2段階に
おいて適正条件でスラブを加熱すると、スケール疵発生
率は1%まで低減された。
Further, as is apparent from the results of Comparative Example 6 (SUS430), when the slab is heated to a temperature range of 1150 ° C. or higher without heating in the first stage, the scale flaw generation rate increases to 30%. On the other hand, as is apparent from the results of Example 7, when the slab was heated under appropriate conditions in the first and second stages, the scale flaw occurrence rate was reduced to 1%.

【0035】さらに、比較例7(SUS329J3L)
の結果から明らかなように、第1段階加熱することな
く、いきなり1200℃以上の温度域にスラブを加熱す
るとスケール疵発生率は33%に増加する。これに対し
て実施例8の結果から明らかなように、第1段階及び第
2段階において適正条件でスラブを加熱すると、スケー
ル疵発生率は1%まで低減された。
Further, Comparative Example 7 (SUS329J3L)
As is clear from the results, when the slab is heated to a temperature range of 1200 ° C. or more without heating in the first stage, the scale flaw generation rate increases to 33%. On the other hand, as is apparent from the results of Example 8, when the slab was heated under appropriate conditions in the first and second stages, the scale flaw occurrence rate was reduced to 1%.

【0036】以上のように、本発明の実施例によればオ
ーステナイト系ステンレス鋼(SUS304)、フェラ
イト系ステンレス鋼(SUS430)、2相系ステンレ
ス鋼(SUS32J3L)のいずれの鋼種においてもス
ケール疵発生率は大幅に低減され、極めて良好な表面性
状を得ることができた。
As described above, according to the embodiment of the present invention, the scale flaw generation rate is increased in any of austenitic stainless steel (SUS304), ferritic stainless steel (SUS430), and duplex stainless steel (SUS32J3L). Was significantly reduced, and extremely good surface properties could be obtained.

【0037】[0037]

【表1】 [Table 1]

【0038】[0038]

【発明の効果】従来、ステンレス鋼の表面にスケール疵
が発生すると、疵手入れにより表面性状が著しく損なわ
れると共に、製造工期及び製造コストの増大を招いてい
た。また、スケール疵抑制のためスラブの低温/短時間
加熱を行うと、圧延温度の低下により製造可能寸法に制
約があった。本発明によれば、熱間加工性の制約なくス
ケール疵発生のないステンレス鋼板を製造することが可
能となり、工業上有益な効果が得られる。
Conventionally, when scale flaws are generated on the surface of stainless steel, the surface properties are remarkably impaired by flaw care, and the production period and production cost are increased. In addition, when the slab is heated at a low temperature for a short time to suppress scale flaws, a reduction in the rolling temperature limits the manufacturable dimensions. ADVANTAGE OF THE INVENTION According to this invention, it becomes possible to manufacture a stainless steel plate without scale flaws without restriction of hot workability, and an industrially advantageous effect is obtained.

Claims (1)

(57)【特許請求の範囲】(57) [Claims] 【請求項1】 ステンレス鋼スラブを1000℃乃至1
100℃の温度範囲で1時間乃至3時間にわたり均熱保
持し、さらに前記スラブを1150乃至1250℃の温
度範囲で2時間以上にわたり均熱保持した後に、熱間圧
延することを特徴とするステンレス鋼スラブの熱間圧延
方法。
1. A stainless steel slab of 1000 ° C. to 1 ° C.
A stainless steel, which is soaked in a temperature range of 100 ° C. for 1 hour to 3 hours and further soaked in the temperature range of 1150 ° C. to 1250 ° C. for 2 hours or more, and then hot-rolled. Hot rolling method of slab.
JP32484293A 1993-12-22 1993-12-22 Hot rolling method of stainless steel slab Expired - Fee Related JP2738281B2 (en)

Priority Applications (1)

Application Number Priority Date Filing Date Title
JP32484293A JP2738281B2 (en) 1993-12-22 1993-12-22 Hot rolling method of stainless steel slab

Applications Claiming Priority (1)

Application Number Priority Date Filing Date Title
JP32484293A JP2738281B2 (en) 1993-12-22 1993-12-22 Hot rolling method of stainless steel slab

Publications (2)

Publication Number Publication Date
JPH07178420A JPH07178420A (en) 1995-07-18
JP2738281B2 true JP2738281B2 (en) 1998-04-08

Family

ID=18170286

Family Applications (1)

Application Number Title Priority Date Filing Date
JP32484293A Expired - Fee Related JP2738281B2 (en) 1993-12-22 1993-12-22 Hot rolling method of stainless steel slab

Country Status (1)

Country Link
JP (1) JP2738281B2 (en)

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* Cited by examiner, † Cited by third party
Publication number Priority date Publication date Assignee Title
MXPA05012509A (en) 2003-05-22 2006-02-08 Sumitomo Metal Ind Fe-Cr ALLY BILLET AND METHOD FOR PRODUCTION THEREOF.

Also Published As

Publication number Publication date
JPH07178420A (en) 1995-07-18

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