JPS6264422A - Vertical straightening method for local collapse of long rail - Google Patents
Vertical straightening method for local collapse of long railInfo
- Publication number
- JPS6264422A JPS6264422A JP20433285A JP20433285A JPS6264422A JP S6264422 A JPS6264422 A JP S6264422A JP 20433285 A JP20433285 A JP 20433285A JP 20433285 A JP20433285 A JP 20433285A JP S6264422 A JPS6264422 A JP S6264422A
- Authority
- JP
- Japan
- Prior art keywords
- rail
- heating
- head
- temperature
- dents
- Prior art date
- Legal status (The legal status is an assumption and is not a legal conclusion. Google has not performed a legal analysis and makes no representation as to the accuracy of the status listed.)
- Granted
Links
Landscapes
- Heat Treatment Of Articles (AREA)
- Machines For Laying And Maintaining Railways (AREA)
- Wire Processing (AREA)
Abstract
Description
【発明の詳細な説明】
〔産業上の利用分胃〕
この発明は敷設状態にあるロングレール頭頂面に生じた
局部凹みを取除いて、頭頂面を平坦化するロングレール
局部凹みの縦矯正法に関ずろ。[Detailed Description of the Invention] [Industrial Use] This invention provides a method for vertically correcting local dents in long rails, which flattens the top surface of the long rail by removing the local dents that have occurred on the top surface of the long rail while it is being laid. No matter what.
高速鉄道のレールには、列車の走行安定性2継目騒音の
低減、軌道保守費の軽減などのため、長さ25mの定尺
レールを溶接して、10〜1.5kmに長大化した溶接
ロングレールが使用されている。High-speed railway rails are made by welding regular length rails of 25 m in length to increase the length from 10 to 1.5 km in order to improve train running stability, reduce second joint noise, and reduce track maintenance costs. rails are used.
レールの溶接には7ラツンユ溶接、ガスLL接、エンク
■7−ズアーク溶接あるいはテルミット溶接が用いられ
ているが、いずれの工法でもレール溶接時の加熱により
、レール溶接部附近は工場で製造されたままの均一な性
質を持ったレー/LI:Jキイ部とは異なった性質がノ
jえられる。Rails are welded using 7-ratunyu welding, gas LL welding, arc welding, or thermite welding, but in any of these methods, the heat generated during rail welding causes the area near the rail weld to be manufactured in a factory. Re/LI has uniform properties as it is: It has different properties from the J key part.
第11図は溶接部中心からの距離(In1N )を横軸
に、頭頂面の硬さく HB )を縦軸にとって、フラツ
ンユ溶接でレールの溶接を行ったときの溶接部近傍にお
けるレール頭頂部の硬さ分4jの−・例を示す。図から
明らかなように、溶接時の熱影響の及ばないけ材部は一
定の硬さを示すが、溶接時の熱影響を受けた部分では硬
、)の著しく低下した部分が生じろ。Figure 11 shows the hardness of the top of the rail near the weld when the rail is welded by flat welding, with the horizontal axis representing the distance from the center of the weld (In1N) and the vertical axis representing the hardness of the top surface (HB). An example of Sabu 4j is shown. As is clear from the figure, the part of the brace that is not affected by the heat during welding exhibits a certain level of hardness, but the part that is affected by the heat during welding has a markedly reduced hardness.
レール(jその頭頂向を車輪が転勤通過するので、頭頂
面の車輪と接触する部分が摩耗する。第12図は溶接部
中心からの距離(閑)を横軸に、頭頂向の摩耗量(、、
)を縦軸にとり第11図;こ示した硬さ分布のレール頭
頂面の逆毛22(Q I−ンにおける¥A粍状態を示す
。レール頭頂面の摩耗状態は溶接部以外の母材部ではほ
ぼ平坦であるが、溶接部Mfflではその硬さの変化に
応じた形状に摩耗する。As the wheels pass along the top of the rail (j), the part of the top surface that comes into contact with the wheels wears out. Figure 12 shows the amount of wear in the top direction ( ,,
) on the vertical axis; Fig. 11 shows the condition of the back hair 22 on the top surface of the rail with the hardness distribution shown in this figure. The welded portion Mffl is almost flat, but the welded portion Mffl wears into a shape that corresponds to the change in hardness.
このため、高速列車の走行に際して、レール溶接部の踏
面状態によっては著しい衝撃音を発生するので、列車速
度の維持・増加させるためには、この踏面の微小な凹凸
を除去することか必要となる0、この微小な凹凸は研削
のみで平坦にすることもできるが、凹凸がある限度を超
えると研削量が大きくなって非能率的・不経済である。For this reason, when a high-speed train runs, significant impact noise is generated depending on the condition of the tread of the rail weld, so in order to maintain or increase train speed, it is necessary to remove minute irregularities on the tread. 0. These minute irregularities can be made flat by only grinding, but if the irregularities exceed a certain limit, the amount of grinding becomes large, which is inefficient and uneconomical.
従来、レール頭頂面の微小な凹凸を除去する縦方向のレ
ールツム正法には■大気渇でI/−ルに弾性限界を超え
ろ曲げ荷重を加えて塑性変形せしめる外力や主体とした
矯正法、■外力は枕木との蹄結により拘束力程度にとど
めて、レール頭部あるいは底部をL侍もバーナを用いて
局部的に加熱・冷却して熱塑性変形させる局部的熱処理
矯正法、及び■レール全断面をガスバーナなど適当な器
具を用いてA3変態点以上に加熱し、これに油圧装置等
で外力を加えて矯正する全体加熱矯正法などがある。Conventionally, the vertical rail correction method for removing minute irregularities on the top surface of the rail includes: - An external force that applies a bending load that exceeds the elastic limit of the I/- rail due to atmospheric dryness to cause it to plastically deform; ■ A local heat treatment straightening method in which the head or bottom of the rail is locally heated and cooled using a burner to thermoplastically deform it by tying it with the railroad ties, and the entire cross section of the rail is There is a whole heating straightening method in which the A3 transformation point or higher is heated using a suitable device such as a gas burner, and then an external force is applied to this using a hydraulic device or the like.
■ 外力を主体とした矯正法は油圧装置を用い、常温近
傍で静的曲げを行う方法であって、曲げ変形量の調整が
容易のため矯正後の仕上がり精度は良好である。■ The straightening method mainly using external force uses a hydraulic device to perform static bending at around room temperature, and since the amount of bending deformation can be easily adjusted, the finishing accuracy after straightening is good.
しかし、レールに対応する大きな荷重に耐える剛性が曲
げ装置に要求されるため、曲げ装置が大型となり通常は
工場あるいは基地作業向である。However, since the bending device is required to have the rigidity to withstand the large load corresponding to the rail, the bending device is large in size and is usually used for factory or base work.
これをiiJ t!i2型として作業性を改善しても敷
設して経年したロングレールの矯正には次めような問題
点を生しる場合がある。すなわら経年したレール頭頂面
には糺み削れなどの表面欠陥が存在する場合が多く、こ
のような部分を矯正するため大きな曲げ応力を加えると
応力集中により欠陥が拡大したり、はなはだしい場合に
は脆性破断に至る恐れすらある。This is iiJ t! Even if the workability of the i2 type is improved, the following problems may occur when straightening long rails that have been installed for many years. In other words, the top surface of rails that have aged often has surface defects such as scratches, and if large bending stress is applied to correct such areas, the defects may expand due to stress concentration, or if they are significant, may even lead to brittle fracture.
■ 局部的熱処理矯正法は特別の装置を必要とせず簡便
であるが、矯正量の再現性に乏しく、加熱温度が低いと
矯正できず、逆に加熱温度が高いと焼割れを生じるため
l門度管理が困難であり、矯正精度を高めるためには高
度な熟練を必要とする問題点があった。■ The local heat treatment straightening method is simple and does not require special equipment, but the reproducibility of the amount of straightening is poor, and it cannot be straightened if the heating temperature is low, and conversely, if the heating temperature is high, it causes quench cracking, so it is not recommended. There was a problem in that it was difficult to control the degree of correction, and a high level of skill was required to improve the accuracy of correction.
■ 全体加熱矯正法はリングバーナなどによりレール全
断面が、l″KlWに保持されているため、矯正に要す
る外力は小さくてよい。しかし、敷設されたロングレー
ルの矯正法としては次のような問題点がある。■ In the whole heating straightening method, the entire cross section of the rail is held at l″KlW using a ring burner, etc., so the external force required for straightening is small. However, as a straightening method for long rails that have been laid, the following There is a problem.
第13図は引張試験一度1)を横軸に、引張強さ1Sと
#i4力YS(kg/mm’)を縦軸にとってレールの
引張試験結果を示したものであり、図から明らかなよう
にレール全断面をA3変態点である750℃以上に加熱
すると、λ・−A強庇は小さくなって容易に矯正できる
。しかし、矯正する時のレール一度が設定温度以下の場
合にはレールに引°胚すの軸力が作用し、その扁度差の
著しい状態、例えば矯正する時のレール温度が敷設した
時の温度より40℃低い時の引張り力(引張り軸力/レ
ール断面積)は約10 kg / m m’となる。一
方、レールの全断面を加熱した場合には、第11づ図に
示すように両力YSは7 kg / m m’、引張強
さは9 kg/mm’以十となり、加熱範囲が引張り力
に爾えられなくなり、加熱範囲に凹み、すなわちやせろ
現象も生じろ。このため、冬期の矯正作業は暮しく制約
される。Figure 13 shows the results of the rail tensile test, with tensile test 1) on the horizontal axis and tensile strength 1S and #i4 force YS (kg/mm') on the vertical axis. When the entire rail cross section is heated above 750° C., which is the A3 transformation point, the λ·-A strong eaves become smaller and can be easily corrected. However, if the temperature of the rail during straightening is lower than the set temperature, the axial force of the stretched steel will act on the rail, resulting in a state where there is a significant difference in flatness, for example, the temperature of the rail when straightening is lower than the temperature when it was laid. The tensile force (pulling axial force/rail cross-sectional area) at a temperature 40°C lower is approximately 10 kg/mm'. On the other hand, when the entire cross section of the rail is heated, as shown in Figure 11, the double force YS is 7 kg/mm', the tensile strength is more than 9 kg/mm', and the heating range is equal to the tensile force. It becomes impossible to lose weight, and there is a dent in the heating range, that is, a thinning phenomenon occurs. For this reason, correction work during the winter season is severely restricted.
また、レール全断面加熱後のi<3却を緩やかにすると
、転動荷重を受けて硬化した敷設レール頭頂面の加熱範
囲に欧化部を生じ、この部分が他の部分より選択的に摩
耗が進行し、結果的に矯正(、た個所が短命となる。In addition, if i < 3 after heating the entire rail cross section is made gentler, a curved part will occur in the heating range of the top surface of the installed rail that has hardened under rolling load, and this part will wear more selectively than other parts. The condition progresses, and as a result, the corrected area becomes short-lived.
この発明はかかる問題点を解決するためになされたもの
で、線路閉鎖を行わずに精度の高い縦矯正のてきるロノ
ゲローノ[の縦矯正法を1【多ろことを目的とする。This invention was made in order to solve such problems, and aims to improve Rono Gerono's vertical straightening method, which enables highly accurate vertical straightening without closing the track.
この発明に係るロングレール局部凹みの縦矯正法は、
■ ロングレール頭頂面の局部凹み位置を中心として、
頭部が引張り側になる。L、うにレールJ戊部から外力
を別人てレール長さ2mあたり10〜25−の多歪みを
与え、
■ この状態で圧縮応力を受けているレール底部の長さ
方向をレール高さ±50mの範囲で750℃〜880℃
に加熱したのらに徐l令し、■ 上記レールの加熱・冷
却にあtこり、レール頭部を300℃以下に保持するこ
とにより、ロングレールの局部凹みを矯正する方法であ
る。The vertical correction method for localized dents in long rails according to the present invention is as follows:
The head is on the tension side. L, Apply external force from the shell of the sea urchin rail J and apply a multi-strain of 10 to 25 - per 2 m of rail length. In the range 750℃~880℃
This is a method of correcting local dents in long rails by heating and cooling the rail, and then maintaining the rail head at 300° C. or lower while heating and cooling the rail.
この発明においては、シー)Lに弾性限界内で予歪みを
与えた後、レール底部をA3変態点以上に加熱し、熱塑
性変形させろと共に、レール頭部を300℃以1ζに保
持することによりレール頭偵部の加熱に伴う軟化すなオ
)ち耐摩耗性の低下を防止する。In this invention, after pre-straining the sea) L within the elastic limit, the bottom of the rail is heated above the A3 transformation point to cause thermoplastic deformation, and the rail head is held at 1ζ above 300°C. Prevents softening due to heating of the head part, which in turn prevents a decrease in wear resistance.
以下、第1図に示ずように頭頂iTi 2の1個所又は
連続した2個所に発生した微小な凹み3を持つレール1
を矯正する方法を具体的に説明する。なお第1図におい
て4はレール10頭部、5は腹部、6は底部である。Hereinafter, as shown in FIG.
We will specifically explain how to correct this. In FIG. 1, 4 is the head of the rail 10, 5 is the abdomen, and 6 is the bottom.
まず、第2図(a)に示すように敷設されたレール1の
凹み3を中心として、シーノム締結装:j27を枕木8
の5〜6本分解放し、加肚台9を凹み3の両側の枕木8
の位置に装着ずろ。また作業中列車が走行してもレール
1が横圧により移動(7て軌間拡大をおこさないように
保持具10を加圧台9の両側の枕木8の位置に装着する
。First, as shown in Fig. 2(a), the sea nom fastening device: j27 is connected to the sleeper 8, centering on the recess 3 of the laid rail 1.
Release 5 to 6 pieces of the sleepers 8 on both sides of the recess 3.
Install it in position. In addition, holders 10 are attached to the sleepers 8 on both sides of the pressurizing platform 9 to prevent the rail 1 from moving due to lateral pressure (7) and causing gauge expansion even if the train runs during work.
次に、第2図(b)に示すようにi+b圧ラーう11を
加圧台9の下に設置し、ポース12により接続された油
圧ポンプ13を用いて加圧し、レール1を持ら上げる。Next, as shown in FIG. 2(b), the i+b pressure rail 11 is installed under the pressure table 9, and is pressurized using the hydraulic pump 13 connected by the port 12 to lift the rail 1. .
レール1をレールの長さほぼ2mあたりで持ち上げろJ
ixは第3図に示す凹み深さdと第4図に示す上越しj
luとの和である。凹み深さdは通常05〜20III
II程度であり、上越しMuは実験の結果05曜程+i
が適当である。したがってレール1を持ら上げろjlx
の範囲は、シー・ルの長さ2mあたりで1.0〜25m
となる。160kg/mレー/Lを2m弦で2.5+m
s持ら上げた場合、レーアL頭部4に加えられる引張り
応力はほぼ” kg / ni m’であり、従来の外
力のみで塑性変形させろ矯正法の場合にレール頭部に加
えられる引張り応力約50 kg / +n m’以上
に比して著しく小さくなる。Lift up rail 1 until the rail length is approximately 2m J
ix is the recess depth d shown in Figure 3 and the overhang j shown in Figure 4.
It is the sum with lu. The recess depth d is usually 05~20III
As a result of the experiment, Joetsu Mu is about 05 days + i
is appropriate. Therefore, lift up rail 1
The range is 1.0 to 25 m per 2 m of seal length.
becomes. 160kg/m le/L with 2m string 2.5+m
When it is lifted, the tensile stress applied to the rail head 4 is approximately "kg/ni m', and the tensile stress applied to the rail head in the case of the conventional straightening method in which plastic deformation is performed only by external force is approximately It is significantly smaller than 50 kg/+n m'.
1ノたがってレール1の頭頂面2に札り割れなどの欠陥
が多少存在しても、欠陥の拡大あるいは脆性破屋iの恐
れは生じない。Therefore, even if there is some defect such as a crack in the rail on the top surface 2 of the rail 1, there is no risk of the defect expanding or brittle damage.
上記のようにシーノ[1を持ち上げた状態で、凹み3直
ドのシール底部6に、第2図(C)に示すように底部加
熱用の小4表炉J4を装着し、ガスバーナ15で所定の
濁度に加熱17t:後冷却する。With the seal [1] lifted as described above, a small 4-sided furnace J4 for heating the bottom is attached to the seal bottom 6 of the 3-hole recess as shown in FIG. 2(C), and a gas burner 15 is used to Heating to a turbidity of 17t: After cooling.
上記のように、レール1に子爪1・を与えた状態で、レ
ール底部6の加熱を行うと、L−/仁1ば底部6の熱膨
張が大きいため、下方へ凹形に変形するが、底部6の加
熱範囲では熱塑性変形がおこり、応力緩和6生して、冷
却後には第5図に示すように若干の凸!4rが残留し、
シール1の矯正が行われろ。なお矯正後必要な場合は第
6図に示す、Lうに研削して仕上げる。研削する場合の
1.゛h低差りは−1−0,3〜−0,1#Im /
mとする。As mentioned above, when the rail bottom 6 is heated with the rail 1 provided with the child claws 1, the bottom 6 of the rail 1 deforms downward into a concave shape due to large thermal expansion. , thermoplastic deformation occurs in the heating range of the bottom part 6, stress relaxation 6 occurs, and after cooling there is a slight convexity as shown in Figure 5! 4r remains,
Seal 1 should be corrected. If necessary after correction, finish by grinding in the L shape shown in Figure 6. 1. When grinding.゛H low difference is -1-0,3~-0,1#Im/
Let it be m.
小型力j14で加熱するレール底部の範囲は実験の結果
、5ON用レールで1.00〜200men、 60
kg / mのレールで1.20−220 mm程度、
ずなわら1.−−ルの高さ±50画程度が適当である。As a result of experiments, the range of the bottom of the rail heated by the small force j14 was 1.00 to 200 men for 5ON rails, 60
kg/m rail about 1.20-220 mm,
Zunawara 1. --The appropriate height is approximately ±50 strokes.
この加熱するレール底部の範囲が狭いと矯正が充分に行
われず、逆にこの範囲が広ずぎると座屈を生じてしまう
。If the range of the bottom of the rail to be heated is narrow, correction will not be performed sufficiently, and conversely, if this range is too wide, buckling will occur.
また、レール断mlにおける最高加熱温度は底部6で7
50〜880℃、頭部4では300℃以下である、。In addition, the maximum heating temperature in the rail section ml is 7 at the bottom 6.
50 to 880°C, and 300°C or less at the head 4.
底部6を750℃以上に加熱するのは、レール鋼(C;
O1i〜0.75%)で(、iΔ3変態点である750
℃以」二で降伏点が極めて小さくなり、変形抵抗を失っ
た状態となって容易に熱塑性変形を化1シろためである
5、逆に750℃以ドては変形抵抗りく大きく、十分な
矯正を行うことが田畑である。The bottom part 6 is heated to 750°C or higher using rail steel (C;
O1i~0.75%) and (,iΔ3 transformation point is 750
At temperatures below 750°C, the yield point becomes extremely small, resulting in a state where the deformation resistance is lost and thermoplastic deformation easily occurs. Tabata is to perform correction.
収部6の加熱)一度の4二限を880℃としたのは、レ
ール鋼を焼ならし一度の最高温度880℃以上に加熱ず
ろと結晶が和犬化して材質が劣化し、もろくなると同時
に収部6を880℃以上の47品にずろとレール頭部4
1i!300℃以−ドに保持ずろことが困fltとなる
ためである。The reason why we set the maximum temperature of 880°C for one time (heating of storage section 6) is that if we normalize the rail steel and heat it to a maximum temperature of 880°C or higher, the crystals will form and the material will deteriorate and become brittle. The storage section 6 is equipped with 47 items with a temperature of 880℃ or higher, and the rail head 4
1i! This is because it becomes difficult to maintain the temperature above 300°C.
レール頭部4 ts230 Q℃以丁に加熱するのは、
第13図に示すように300℃以下では引張強さr s
、 rq4力YSの低下が起きなく、転動荷重で硬化
されたシール頭頂面2に欧化部が発生せず、M六↓・L
性が損なわれないためである。Rail head 4 TS230 Heating to Q℃ is as follows:
As shown in Figure 13, below 300°C, the tensile strength r s
, rq4 force YS does not decrease, no Europeanized part occurs on the seal top surface 2 hardened by rolling load, and M6↓・L
This is because the sex is not impaired.
第7図は加熱開始からの時間1m1n)を横軸に、lム
f1.f (℃l を縦軸にとって、レール1を加熱・
冷却したときの1・−ル各部の加熱・冷却曲線の一例を
示す。図に示した加熱・冷却曲線はレール温度が6〜1
2℃の場合てあり、aは頭頂面、bl、を収部中心、C
は底部中心の加熱・冷却曲線である。In FIG. 7, the time from the start of heating (1m1n) is plotted on the horizontal axis, and lmf1. f (Heating rail 1, taking ℃l as the vertical axis)
An example of the heating/cooling curve of each part of the 1.-ru when cooled is shown. The heating/cooling curve shown in the figure shows the rail temperature between 6 and 1.
In the case of 2℃, a is the parietal surface, bl is the center of the acquisition area, and C
is the heating/cooling curve centered at the bottom.
この加熱・冷却曲線は、まず小梨炉14でレール底部6
を加熱(7、レール底部6が1すf定のt昂度例左ば7
50℃に達した時にガスバーナ15を消火し、その後炉
冷及び空冷に」、り徐冷し、レール底部6の温度が30
0℃程度に達しl・ら水冷する。This heating/cooling curve is first applied to the rail bottom 6 at the Konashi furnace 14.
Heating (7, rail bottom 6 is 1 f constant t exaltation example left 7)
When the temperature reached 50°C, the gas burner 15 was extinguished, and then the temperature at the bottom of the rail 6 reached 30°C.
Once it reaches about 0°C, cool it with water.
この加熱・冷却の際シールH1部5の最高加熱温度は5
00℃以下、頭頂面2の最14加熱;品度は300℃9
.下である。During this heating and cooling, the maximum heating temperature of the seal H1 part 5 is 5
00℃ or less, maximum heating of top surface 2; quality is 300℃9
.. It's below.
上記のようにレール底部6の温度が750℃。As mentioned above, the temperature of the rail bottom 6 is 750°C.
腹部5の一度が500℃以下2頭頂1fj2の一度が3
00℃以下の場合、レール1の耐力は約25kg/ m
m’、引張強さは約45 kg / nn m’とな
り、設定温度からマイナス40℃の冬期においてもレー
ル強度は約10kg/+nm’となる引張り力(引張り
軸力/レール断面8りをはるかに超えて安全である。Once in the abdomen 5 is below 500℃ 2 Once in the top of the head 1 fj 2 is 3
When the temperature is below 00℃, the proof strength of rail 1 is approximately 25kg/m
m', the tensile strength is approximately 45 kg / nn m', and even in winter when the temperature is -40°C from the set temperature, the rail strength is approximately 10 kg / +nm'. It is safe beyond all limits.
次に上記実施例により具体的にレール1を矯正しtこ結
果を示す。Next, we will show the results of straightening the rail 1 in detail according to the above embodiment.
高速鉄道に長年敷設使用した60kg/mのロノグレー
ルの不動区間に生じた頭Ia面2の凹みを矯正した。こ
の矯正において、枕木の締結装置緊解本数は6本、レー
ル温度はおおむね6〜12℃で、シー ルの加熱・冷却
はレールJ戊部6の加熱範囲を約200調とし、第7図
に示した加熱冷却曲線を適用して行った。Corrected the dent on the head Ia surface 2 that occurred in the stationary section of the 60kg/m Ronograil that had been installed and used for many years on high-speed railways. In this correction, the number of tightening devices for the sleepers was 6, the rail temperature was approximately 6 to 12°C, and the heating and cooling range of the seal was set to about 200 degrees at the rail J hole 6, as shown in Figure 7. The heating and cooling curves shown were applied.
乙のL−/lのM矯正の際、第8図に示すレールの長さ
L = 2 cnあなりの持ら」二げる量x (nu+
+ 72m )と矯正基y (1oI11/2m )
との関係を第9図に示す。When correcting M of L-/l, the length of the rail shown in Figure 8 L = 2 cn
+72m) and correction group y (1oI11/2m)
Figure 9 shows the relationship between
持らLげる旦Xと矯正Myとの直線的傾向(よ回帰式y
=1.095に−0,537てあられされ、相関係数r
!、tO,908てあり、持ち上げろ呈Xと矯正基yと
は、はぼ完全な相関を示し矯正精度はきわめて高い。A linear tendency between the lifting force X and the correction My (regression equation y
= 1.095 -0,537 hail, correlation coefficient r
! , tO, 908, and the lifting force X and the correction base y show an almost perfect correlation, and the correction accuracy is extremely high.
また第10図に溶接部中心からの距離(閤)を横軸に硬
さ (1(sl を縦軸にとって、矯正l1il後のり
fi rrs 1rii 2各部の硬さを示す。?51
0図に示すように頭Iff im 2は加熱による硬さ
変化が生じなく、矯L 後J+矯正前の硬さを保持する
ことができろ。In addition, Fig. 10 shows the hardness of each part after straightening, with the horizontal axis representing the distance from the center of the weld (1 (sl)) and the vertical axis.
As shown in Figure 0, the hardness of the head If im 2 does not change due to heating, and it can maintain the hardness of J+ before orthodontic treatment after orthodontic treatment.
この発明は以上説明したように、シーノFに弾性限界内
の予否みを!jえた後、レール底部をA3変態点以上に
加熱17熱塑性変形させろと共に、レール頭部を300
℃以下に保持してレールの縦矯正を行うから、m正の際
もシー・1が充分な引張強さ。As explained above, this invention provides SEENO F with predictions within the elastic limit! After heating, heat the bottom of the rail to a temperature above the A3 transformation point to thermoplastically deform it, and heat the top of the rail to a temperature of 300°C.
Because the rail is vertically straightened by keeping it below ℃, C.1 has sufficient tensile strength even when m is positive.
耐力を有し、従来の矯正方法でしばしば発生しt−レー
ル断面積の減少なしで、かつ線路閉鎖を行わずに精度の
高い′ctI)j!正を行うことができろ3、また矯正
後もレール頭頂面の硬さに変化が生じないから、レール
頭頂面の耐;や肝性を保持することができる。ctI)j! with high precision without reducing the T-rail cross-sectional area and without track closure, which often occurs with conventional straightening methods! Since the hardness of the rail parietal surface does not change even after correction, the durability and strength of the rail parietal surface can be maintained.
さらに、レール頭部に大きな引張応力を与えないから、
頭頂面に存在した微小な疵の拡大も防+hできる効果を
有ずろ。Furthermore, since it does not apply large tensile stress to the rail head,
It also has the effect of preventing the expansion of minute flaws that existed on the top of the head.
第1図はシーノLの↑)視図、第2図(al、(b)。
(cr、(d)+よこの発明の′A施例の説明図であり
、第2図(a)は平向図、第2図(blは第2図(al
のΔ−A断面図、第2図(c)は第2図(ハ)のF3−
3断面図、第214(d)は第2図(alのC−C断面
図。
第3図〜第6図は上記実施例の動作説明図、第7図は加
熱・冷却曲線の分布図、第8図は持も上げろに!、Xと
矯正斌yの説明図、第9図は持ら上げる(荻Xと)U
+’E 、m yの持告図、第10図は頭頂向硬4\分
4i図、第11図(よロンゲ1−一−・L溶に時のレー
ル頭ro、 1iIIの硬さ分III l!”4、第1
2図は溶接部の明耗斌分市図、第1 :(1j−41i
、I L−ルの温度−づしπ2強さ、Il〕J力持性ト
4である。
1・ レール、2;頭頂部、3:凹y本、4:頭部、1
′) 代部。
代理人 プC理上 佐 藤 止 集
第1図
第2図
t^1
腸
(b) (c) (d)第3図
范 4図
第 6図
り
第7図
刀t7里にr4十隻市らりy斗ハJ’i (mint
第 8文
第 9図
騎二ヴ)量x(mm/2m)
第10図
斜仰t7b*”=f)i!k (mm)第11図
第 12 vl
奏ルr外・h゛鋤旺鯰(mrr+)
第 13図Figure 1 is an ↑) perspective view of Seeno L, Figure 2 (al, (b)) is an explanatory diagram of the 'A embodiment of this invention (cr, (d) + side), and Figure 2 (a) is Plan view, Figure 2 (bl is Figure 2 (al)
The Δ-A sectional view of FIG. 2(c) is the F3-A cross-sectional view of FIG. 2(c).
3 sectional view, 214(d) is a C-C sectional view of FIG. Figure 8 is an explanatory diagram of ``Hold it up!''
+'E,my's holding diagram, Figure 10 is the parietal direction hardness 4\min 4i diagram, Figure 11 (Yoronge 1-1-・L melting time rail head ro, 1iII hardness part III l!”4, 1st
Figure 2 is a map of the welding area, No. 1: (1j-41i
, I L - Temperature of L - π2 Strength, Il] J Strength 4. 1. Rail, 2; Top of head, 3: Concave Y book, 4: Head, 1
') Daibe. Agent PuC Rijo Sato Toshi Collection Figure 1 Figure 2 t^1 Intestine (b) (c) (d) Figure 3 Fan 4 Figure 6 Figure 7 Sword t7 Ri to r4 Jifuneichi et al. RiyatohaJ'i (mint
8th sentence, Figure 9, weight x (mm/2m) Figure 10, diagonal elevation t7b*”=f) i!k (mm) Figure 11, 12 vl outside r, h (mrr+) Figure 13
Claims (3)
、頭部が引張り側になるようにレール底部から外力を与
えて、レール長さ2mあたり1.0〜2.5mmの予歪
みを与え、 この状態で、圧縮応力を受けているレール底部の長さ方
向をレール高さ±50mmの範囲を加熱炉でおおい75
0℃〜880℃に加熱した後徐々に冷やし、熱塑性変形
をさせるロングレール局部凹みの縦矯正法。(1) Centering around the local concave position on the top surface of the long rail, apply an external force from the bottom of the rail so that the head is on the tension side to give a pre-strain of 1.0 to 2.5 mm per 2 m of rail length, In this state, the length direction of the bottom of the rail, which is under compressive stress, is covered with a heating furnace within ±50 mm of the rail height.
A vertical correction method for localized dents in long rails, which involves heating to 0°C to 880°C and then gradually cooling to cause thermoplastic deformation.
300℃以下に保持する特許請求の範囲第1項記載のロ
ングレール局部凹みの縦矯正法。(2) The method for vertically correcting local dents in a long rail according to claim 1, wherein the rail head is maintained at 300° C. or lower during heating and cooling of the rail.
ルの局部凹みを矯正する特許請求の範囲第1項及び第2
項記載のロングレール局部凹みの縦矯正法。(3) If necessary, the top of the rail head is further ground to correct local dents in the rail. Claims 1 and 2
Vertical correction method for localized dents in long rails as described in Section 1.
Priority Applications (1)
Application Number | Priority Date | Filing Date | Title |
---|---|---|---|
JP20433285A JPH0238043B2 (en) | 1985-09-18 | 1985-09-18 | RONGUREERUKYOKUBUHEKOMINOTATEKYOSHOBO |
Applications Claiming Priority (1)
Application Number | Priority Date | Filing Date | Title |
---|---|---|---|
JP20433285A JPH0238043B2 (en) | 1985-09-18 | 1985-09-18 | RONGUREERUKYOKUBUHEKOMINOTATEKYOSHOBO |
Publications (2)
Publication Number | Publication Date |
---|---|
JPS6264422A true JPS6264422A (en) | 1987-03-23 |
JPH0238043B2 JPH0238043B2 (en) | 1990-08-28 |
Family
ID=16488741
Family Applications (1)
Application Number | Title | Priority Date | Filing Date |
---|---|---|---|
JP20433285A Expired - Lifetime JPH0238043B2 (en) | 1985-09-18 | 1985-09-18 | RONGUREERUKYOKUBUHEKOMINOTATEKYOSHOBO |
Country Status (1)
Country | Link |
---|---|
JP (1) | JPH0238043B2 (en) |
Cited By (3)
Publication number | Priority date | Publication date | Assignee | Title |
---|---|---|---|---|
CN102266880A (en) * | 2011-07-07 | 2011-12-07 | 徐州开元世纪重型锻压有限公司 | Moving operating platform for rail correcting hydraulic press |
CN107952826A (en) * | 2017-11-17 | 2018-04-24 | 中冶陕压重工设备有限公司 | A kind of high ferro rail or railway frog straightening equipment and its method for aligning |
CN109530489A (en) * | 2018-12-04 | 2019-03-29 | 合肥合锻智能制造股份有限公司 | A kind of mobile work platform for heel end track switch |
-
1985
- 1985-09-18 JP JP20433285A patent/JPH0238043B2/en not_active Expired - Lifetime
Cited By (4)
Publication number | Priority date | Publication date | Assignee | Title |
---|---|---|---|---|
CN102266880A (en) * | 2011-07-07 | 2011-12-07 | 徐州开元世纪重型锻压有限公司 | Moving operating platform for rail correcting hydraulic press |
CN107952826A (en) * | 2017-11-17 | 2018-04-24 | 中冶陕压重工设备有限公司 | A kind of high ferro rail or railway frog straightening equipment and its method for aligning |
CN107952826B (en) * | 2017-11-17 | 2020-04-24 | 中冶陕压重工设备有限公司 | Straightening equipment for high-speed rail or frog and straightening method thereof |
CN109530489A (en) * | 2018-12-04 | 2019-03-29 | 合肥合锻智能制造股份有限公司 | A kind of mobile work platform for heel end track switch |
Also Published As
Publication number | Publication date |
---|---|
JPH0238043B2 (en) | 1990-08-28 |
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