JPH067877A - Forging method for aluminum alloy - Google Patents

Forging method for aluminum alloy

Info

Publication number
JPH067877A
JPH067877A JP19294292A JP19294292A JPH067877A JP H067877 A JPH067877 A JP H067877A JP 19294292 A JP19294292 A JP 19294292A JP 19294292 A JP19294292 A JP 19294292A JP H067877 A JPH067877 A JP H067877A
Authority
JP
Japan
Prior art keywords
forging
shape
scroll
thickness
die
Prior art date
Legal status (The legal status is an assumption and is not a legal conclusion. Google has not performed a legal analysis and makes no representation as to the accuracy of the status listed.)
Pending
Application number
JP19294292A
Other languages
Japanese (ja)
Inventor
Koji Nakamura
康二 中村
Yoji Hosono
洋司 細野
Current Assignee (The listed assignees may be inaccurate. Google has not performed a legal analysis and makes no representation or warranty as to the accuracy of the list.)
Nippon Light Metal Co Ltd
Original Assignee
Nippon Light Metal Co Ltd
Priority date (The priority date is an assumption and is not a legal conclusion. Google has not performed a legal analysis and makes no representation as to the accuracy of the date listed.)
Filing date
Publication date
Application filed by Nippon Light Metal Co Ltd filed Critical Nippon Light Metal Co Ltd
Priority to JP19294292A priority Critical patent/JPH067877A/en
Publication of JPH067877A publication Critical patent/JPH067877A/en
Pending legal-status Critical Current

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  • Rotary Pumps (AREA)
  • Forging (AREA)

Abstract

PURPOSE:To provide a forged scroll product having an excellent shape characteristic and no underfill and unequal thickness, etc., by softening a work hardened material in the state set in a die. CONSTITUTION:When the scroll having a ratio H/T >=5 of tooth height H to tooth thickness T is forged, almost entire target shape of the product is formed by pressing the maternal up to a specific pressure P1 determined by the ratio H/T. The material set in the die is held for a specific time t1-t2 keeping the load applied on it and softened by working heat. Then, after a little reduction of pressing force from P1 to P2, the material is formed in the final shape by increasing the load again. Thus, since the work hardened material is softened utilising working heat in the state set in the die, a scroll product having a complex shape is manufactured without requiring high pressure and intermediate annealing.

Description

【発明の詳細な説明】Detailed Description of the Invention

【0001】[0001]

【産業上の利用分野】本発明は、アルミニウム合金の鍛
造によって複雑形状の製品を製造する方法に関する。
BACKGROUND OF THE INVENTION 1. Field of the Invention The present invention relates to a method for producing a product having a complicated shape by forging an aluminum alloy.

【0002】[0002]

【従来の技術】コンプレッサーに組み込まれるスクロー
ルは、図1に示すように円板状のフランジ1にヘリカル
状のラップ部分2が一体的に形成されている。ラップ部
分2は、高さが20mmを超え、幅が4mm程度の薄く
長い形状をもっている。また、この種の部品に要求され
る低い熱膨張係数,高強度,耐摩耗性等を得るため、高
Siのアルミニウム合金が使用されている。
2. Description of the Related Art In a scroll incorporated in a compressor, as shown in FIG. 1, a disc-shaped flange 1 is integrally formed with a helical wrap portion 2. The wrap portion 2 has a thin and long shape with a height of more than 20 mm and a width of about 4 mm. Further, in order to obtain a low coefficient of thermal expansion, high strength, wear resistance, etc. required for this type of component, a high Si aluminum alloy is used.

【0003】高Siアルミニウム合金の鍛造によって図
1に示すような複雑形状の部品を得ようとすると、形状
に由来する高い摩擦抵抗及び材質に由来する変形抵抗か
ら、鍛造が極めて困難な作業となる。鍛造を容易にする
手段としては、一般的に潤滑剤の改良や熱間加工によっ
て材質の変形抵抗を小さくした状態で鍛造を行うこと等
が掲げられる。しかし、局部的な変形が著しいアルミニ
ウム合金の鍛造にあっては、変形速度も考慮に入れた鍛
造が必要となる。これらの点から、黒鉛系の潤滑剤を使
用し、400℃以上の高温に保持したアルミニウム合金
を18〜66m/分程度の比較的ゆっくりとしたラム速
度で最終圧まで加圧する方法が採用されている。
When a component having a complicated shape as shown in FIG. 1 is to be obtained by forging a high Si aluminum alloy, forging becomes an extremely difficult work due to the high frictional resistance derived from the shape and the deformation resistance derived from the material. . As means for facilitating forging, generally, forging is performed in a state where the deformation resistance of the material is reduced by improving the lubricant or hot working. However, in the forging of an aluminum alloy that is significantly deformed locally, it is necessary to take the forging taking into account the deformation rate. From these points, a method of using a graphite-based lubricant and pressurizing an aluminum alloy held at a high temperature of 400 ° C. or higher to a final pressure at a relatively slow ram speed of about 18 to 66 m / min is adopted. There is.

【0004】[0004]

【発明が解決しようとする課題】特に複雑な形状をもつ
製品を得ようとする場合、従来の鍛造法では欠肉,偏肉
等が生じ易い。これは、ラップ2の先端まで十分な材料
の塑性流動が鍛造時に生じないことに起因する。
Particularly when a product having a complicated shape is to be obtained, the conventional forging method is apt to cause lack of thickness, uneven thickness and the like. This is because sufficient plastic flow of the material to the tip of the wrap 2 does not occur during forging.

【0005】たとえば、図2に示すように、フランジ1
の端面1aからラップ2aまでの距離L1 が十分に大き
いとき、ラップ2aの先端まで肉の供給が行われる。こ
の場合、ラップ2aに相当する金型キャビティの全体に
肉が行き渡り、所期形状のラップ2aが形成される。他
方、フランジ端面1bから近い距離L2 に位置するラッ
プ2bでは、フランジ1から肉の補給が十分でなく、欠
肉が生じる。欠肉した部分では、ラップ2の高さや肉厚
が不足する。この種の欠肉は、ラップ2の巻き始め2s
や巻き終り2eに発生し易く、歯厚に比較して歯高が5
倍以上のスクロールで顕著にみられる。
For example, as shown in FIG. 2, the flange 1
When the distance L 1 from the end face 1a to the wrap 2a is sufficiently large, the meat is supplied to the tip of the wrap 2a. In this case, the meat is spread over the entire mold cavity corresponding to the wrap 2a, and the wrap 2a having the desired shape is formed. On the other hand, the wrap 2b located at a distance L 2 near the flange end face 1b, supply from the flange 1 of the meat is not sufficient, the underfill occurs. The height and the wall thickness of the wrap 2 are insufficient in the part where the meat is cut. This kind of flesh is the beginning of the wrap 2 2s
It tends to occur at the end of winding and 2e, and the tooth height is 5 compared to the tooth thickness.
It is noticeable when scrolling more than twice.

【0006】フランジ1からラップ2に肉を補給して欠
肉を避けるため、フランジ1を薄肉化することが考えら
れる。しかし、フランジ1の薄肉化には、極めて大きな
荷重が要求される。すなわち、他の部分にあるラップ2
に相当する金型キャビティは、フランジ1から塑性流動
した肉がすでに充満されており、荷重を更に上昇させて
も変形は望めない。この状況下で巻き始め2sや巻き終
り2e等のラップ2に欠肉を解消する肉を、加圧力で薄
肉化したフランジ1から補給しようとすることは実際上
不可能である。
It is conceivable to thin the flange 1 in order to replenish the lap 2 with the meat from the flange 1 to avoid the lack of thickness. However, an extremely large load is required to reduce the thickness of the flange 1. That is, the wrap 2 in the other part
The mold cavity corresponding to (3) is already filled with the plastically flowed meat from the flange 1, and deformation cannot be expected even if the load is further increased. Under this circumstance, it is practically impossible to try to replenish the wrap 2 such as the winding start 2s and the winding end 2e for removing the thickness of the wrap 2 from the thinned flange 1 by pressing force.

【0007】加工硬化した素材は、中間焼鈍によって軟
質化することができる。しかし、中間焼鈍を採用する場
合、加工途中の素材を金型から取り出し、軟質化後の素
材を再度金型にセットする作業が必要になる。そのた
め、作業工数が大幅に増加し、作業性,生産性の低下を
招く。本発明は、このような問題を解消すべく案出され
たものであり、金型から素材を鍛造途中で取り出すこと
なく鍛造を2段階で行うことによって、金型キャビティ
の隅々まで肉を充満させ、欠肉,偏肉等のない形状特性
に優れた製品を得ることを目的とする。
The work-hardened material can be softened by intermediate annealing. However, when the intermediate annealing is adopted, it is necessary to take out the material being processed from the mold and set the softened material in the mold again. As a result, the number of man-hours required for working increases significantly, leading to a drop in workability and productivity. The present invention has been devised to solve such a problem, and by performing forging in two stages without taking out the material from the die during forging, the meat is filled in every corner of the die cavity. The purpose is to obtain a product with excellent shape characteristics without lacking thickness, uneven thickness, and the like.

【0008】[0008]

【課題を解決するための手段】本発明の鍛造方法は、そ
の目的を達成するため、歯高H及び歯厚TがH/T≧5
の形状をもつスクロールに対応したキャビティを有する
金型にアルミニウム合金素材をセットし、該素材の材
質,製品の形状,加工温度等によって定まる所定圧力ま
で加圧することにより、目標形状のほぼ全体を成形する
第1鍛造工程、そのままのプレス位置で前記素材を保持
する保持工程、及び加圧力が若干低下した後で加圧力を
再度上昇させて最終形状に成形する第2鍛造工程を備え
ていることを特徴とする。
In order to achieve the object, the forging method of the present invention has a tooth height H and a tooth thickness T of H / T ≧ 5.
Almost all of the target shape is formed by setting the aluminum alloy material in the mold that has the cavity corresponding to the scroll of the shape and pressurizing to a predetermined pressure determined by the material of the material, the shape of the product, the processing temperature, etc. A first forging step, a holding step of holding the raw material at the pressing position as it is, and a second forging step of forming the final shape by increasing the pressing force again after the pressing force has slightly decreased. Characterize.

【0009】[0009]

【作 用】歯高H及び歯厚TがH/T≧5の形状をもつ
スクロールに対応したキャビティを有する金型にアルミ
ニウム合金素材をセットしてスクロールを鍛造すると
き、金型に加えられる荷重は、図3に示すように変化す
る。時点t1 まで、ほぼ一定した速度で荷重を増加させ
る。同じ材質に関しては比H/Tで定まる加圧力P1
達したA点で、金型キャビティのほぼ全体に素材が塑性
流動している。この素材は、多数の転位の導入によって
加工硬化している。そのため、荷重を更に増加させるこ
とは困難であり、素材は変形しにくい状態になってい
る。また、比H/T≧5では、急速に巻き始め及び巻き
終りの部分における成形性が悪くなる。そのため、A点
以上に荷重を増加させても、欠肉,偏肉等の欠陥発生が
解消されない。
[Working] The load applied to the die when the aluminum alloy material is set in a die having a cavity corresponding to the scroll having a tooth height H and tooth thickness T of H / T ≧ 5 and the forging of the scroll is performed. Changes as shown in FIG. The load is increased at a substantially constant rate until time t 1 . With respect to the same material, at point A when the pressing force P 1 determined by the ratio H / T is reached, the material is plastically flowed to almost the entire mold cavity. This material is work hardened by the introduction of many dislocations. Therefore, it is difficult to further increase the load, and the material is in a state of being difficult to deform. On the other hand, if the ratio H / T ≧ 5, the formability at the beginning and the end of the winding becomes poor. Therefore, even if the load is increased above the point A, defects such as lack of thickness and uneven thickness cannot be eliminated.

【0010】A点のプレス位置をそのまま保持しておく
と、荷重が若干下降する現象がみられる。この現象は、
加工熱によって素材が昇温し軟質化することに起因する
ものと推察される。荷重が加圧力P2 まで減少する過程
で、素材の軟質化に伴って転位が回復する。その結果、
B点に至った素材は、変形抵抗が低下し加工し易いもの
となる。
If the pressing position at point A is kept as it is, a phenomenon in which the load is slightly lowered is observed. This phenomenon is
It is speculated that this is due to the fact that the material heats up and softens due to the processing heat. In the process in which the load is reduced to the pressing force P 2 , the dislocation is recovered as the material softens. as a result,
The material reaching point B has a low deformation resistance and is easy to process.

【0011】保持時間t1 〜t2 は、比H/Tに応じて
変わるものであり、比H/Tが大きくなるほど長く設定
することが必要である。たとえば、比H/Tが5〜7の
範囲にあるとき、保持時間t1 〜t2 は10〜12秒の
範囲で適宜定められる。また、素材の軟質化を効果的に
進行させるため、このの間の素材を450〜470℃の
温度範囲に維持することが好ましい。軟質化された素材
に対し更にC点まで荷重を増加させ、最終形状に鍛造す
る。この第2鍛造工程では、第1鍛造工程で変形しにく
かった部分の変形抵抗が低下しており、金型キャビティ
の隅々まで素材が塑性流動する。そのため、図1に示し
たスクロールのような複雑形状であっても、欠肉や偏肉
のない形状特性に優れた製品が得られる。昇圧時間t2
〜t3 は、特に本発明を拘束するものではないが、たと
えば第1鍛造工程と同様な昇圧速度でC点まで達するよ
うな時間に設定することができる。
The holding times t 1 to t 2 vary depending on the ratio H / T, and it is necessary to set the holding time longer as the ratio H / T increases. For example, when the ratio H / T is in the range of 5 to 7, the holding time t 1 to t 2 is appropriately set in the range of 10 to 12 seconds. Further, in order to effectively progress the softening of the material, it is preferable to maintain the material in the meantime in the temperature range of 450 to 470 ° C. The load is further increased to point C for the softened material, and it is forged into the final shape. In this second forging step, the deformation resistance of the portion that was difficult to deform in the first forging step is reduced, and the material plastically flows to every corner of the mold cavity. Therefore, even if it has a complicated shape such as the scroll shown in FIG. 1, it is possible to obtain a product excellent in shape characteristics without lacking thickness or uneven thickness. Boosting time t 2
Although not particularly restricted to the present invention, t 3 to t 3 can be set to a time such that, for example, the point C is reached at the same pressurizing speed as in the first forging step.

【0012】すなわち、本発明においては、第1鍛造工
程で発生した加工熱を素材の昇温・軟質化に利用し、金
型に素材をセットしたままの状態で第2段階の鍛造を行
うことにより、複雑形状をもつ製品を良好な作業性で製
造している。この点、中間焼鈍を伴う従来の鍛造法にあ
っては、A点に至った素材を金型から一旦取り外し、熱
処理によって軟化した後で金型に再度セットして鍛造を
行っている。この従来法と比較するとき、本発明に従っ
た2段鍛造が作業性,熱経済等に優れていることが歴然
としている。また、最終形状に成形する第2鍛造工程に
おいても、比較的小さな荷重で鍛造することができるた
め、小型プレスの使用が可能になると共に、金型の寿命
も延長する。保持工程における荷重の低下は、プレスの
負荷を測定することにより簡単に検出される。そこで、
荷重が低下した時点で再度荷重を増加させるシーケンス
を組むとき、通常の1段鍛造と実質的に同様な作業プロ
セスとすることができる。
That is, in the present invention, the working heat generated in the first forging step is used for raising the temperature and softening the material, and the second stage forging is performed with the material set in the die. Manufactures products with complex shapes with good workability. In this respect, in the conventional forging method involving intermediate annealing, the material reaching point A is once removed from the mold, softened by heat treatment, and then set in the mold again for forging. When compared with this conventional method, it is obvious that the two-step forging according to the present invention is excellent in workability, thermal economy and the like. Also, in the second forging step for forming the final shape, it is possible to forge with a relatively small load, so that a small press can be used and the life of the die is extended. The decrease in load during the holding process is easily detected by measuring the load on the press. Therefore,
When a sequence of increasing the load again when the load is reduced is performed, the working process can be substantially the same as that of the normal one-step forging.

【0013】加圧力P1 ,P2 及び時点t1 〜t3 は、
素材の材質,製品形状,鍛造温度等に応じて変わるもの
であり、一概に定めることはできない。ただし、加圧力
1は、製品形状のほぼ全体が成形されることを目安と
して決定される。また、加圧力P2 及び時間t1 〜t2
は、第1段階の鍛造によって加工硬化した素材の変形抵
抗を減少させ、第2段階の鍛造を容易にすることを狙っ
て決定される。第2鍛造工程における最高到達荷重であ
る加圧力P2 は、特に制約されるものではないが、プレ
スの能力を考慮するとき加圧力P1 とほぼ同程度とする
ことが好ましい。第2段階の鍛造によっても加工硬化が
激しい場合には、保持工程を再度経由した後、鍛造を繰
り返す。この保持工程を間においた鍛造の繰返しによっ
て、複雑な形状をもつ製品であっても、欠肉,偏肉等の
欠陥がなく優れた形状特性に仕上げることができる。
The applied pressures P 1 and P 2 and the times t 1 to t 3 are
It varies depending on the material quality, product shape, forging temperature, etc., and cannot be specified unconditionally. However, the pressing force P 1 is determined on the basis that almost the entire product shape is molded. Further, the pressing force P 2 and time t 1 to t 2
Is determined with the aim of reducing the deformation resistance of the work-hardened material by the first stage forging and facilitating the second stage forging. The pressing force P 2 which is the maximum ultimate load in the second forging step is not particularly limited, but it is preferable that it is substantially the same as the pressing force P 1 when considering the capability of the press. If the work hardening is severe even by the forging in the second stage, the forging is repeated after passing through the holding step again. By repeating forging with this holding step in between, even a product having a complicated shape can be finished with excellent shape characteristics without defects such as lack of thickness or uneven thickness.

【0014】[0014]

【実施例】Si:10.5%,Mn:0.5%,Cu:
3.0%,Mg:0.5%及びSb:0.2%を含むア
ルミニウム合金の押出し棒(直径125mm)から、厚
さ25mmの素材を切り出した。素材の表面に黒鉛系の
潤滑剤を塗布した後、450℃に加熱する熱処理を施
し、予め250℃に保持した金型にセットした。そし
て、加圧力P1 =600トン (50kg/mm2)及びP
2 =500トン(40kg/mm2)とする荷重で鍛造す
ることにより、厚み12mm及び直径130mmのフラ
ンジ1の一面に歯厚T=5mm,歯高H=35mm及び
長さ520mmのラップ2がスパイラル状に起立し、フ
ランジ1の他面にボス3が設けられているスクロールを
製造した。フランジ1の端面1bからフィン2bまでの
最短距離L2 (図2参照)を、7mmとした。
EXAMPLES Si: 10.5%, Mn: 0.5%, Cu:
A 25 mm thick material was cut out from an extruded rod (diameter 125 mm) of an aluminum alloy containing 3.0%, Mg: 0.5% and Sb: 0.2%. After applying a graphite-based lubricant to the surface of the material, a heat treatment of heating to 450 ° C. was performed and the mold was set in advance at 250 ° C. Then, the pressing force P 1 = 600 tons (50 kg / mm 2 ) and P
By forging with a load of 2 = 500 tons (40 kg / mm 2 ), the wrap 2 having a tooth thickness T = 5 mm, a tooth height H = 35 mm and a length 520 mm is spirally formed on one surface of the flange 1 having a thickness of 12 mm and a diameter of 130 mm. A scroll having a boss 3 formed on the other surface of the flange 1 was manufactured. The shortest distance L 2 (see FIG. 2) from the end surface 1b of the flange 1 to the fin 2b was set to 7 mm.

【0015】A点に到達する時点t1 を20秒に設定
し、ほぼ一定した速度で昇圧し第1鍛造工程を終了し
た。第1鍛造工程後の素材を金型から取り出し、その形
状を観察した。素材には、図4(a)に点線で示す欠肉
部2e'がラップ2の巻き終り2eに発生し、図4(b)
に点線で示す欠肉部2s'が巻き始め2sに発生してい
た。欠肉部2s'は、端部の高さが目標寸法の2/3に当
る20mmで、長手方向に沿って15mmの範囲にわた
りラップ2の高さが不足していた。欠肉部2e'は、端部
の高さが目標寸法より大幅に低い25mmで、長手方向
に沿って15mmの範囲にわたりラップ2の高さが不足
していた。
The time t 1 when reaching the point A was set to 20 seconds, the pressure was increased at a substantially constant speed, and the first forging step was completed. The material after the first forging step was taken out of the mold and its shape was observed. A blank portion 2e ′ shown by a dotted line in FIG. 4 (a) occurs in the material at the winding end 2e of the wrap 2, and FIG.
A flesh portion 2s' indicated by a dotted line was generated in the winding start 2s. In the thickness-reduced portion 2s', the height of the end portion is 20 mm, which corresponds to 2/3 of the target dimension, and the height of the wrap 2 is insufficient over a range of 15 mm along the longitudinal direction. The thickness of the flesh portion 2e 'was 25 mm, which was significantly lower than the target height, and the height of the wrap 2 was insufficient over the range of 15 mm in the longitudinal direction.

【0016】そこで、第1鍛造工程が終了した素材を金
型から取り出すことなく、そのままのプレス位置で時点
2 =32秒まで保持した。保持工程にある素材に対
し、金型に埋め込んだ熱電対によって素材温度の経時的
変化を調べた。その結果、時間t1 〜t2 =12秒の
間、470℃以上の高温に素材が保持されていることが
判った。この保持工程で、プレスの荷重もP1 =600
トンからP2 =500トンまで降下した。加圧力の下降
は、素材温度の上昇によって素材が軟化し、変形抵抗が
減少したことを示す。
Therefore, the material for which the first forging step was completed was held in the pressing position as it was until the time t 2 = 32 seconds without being taken out from the die. With respect to the material in the holding step, the temperature change of the material temperature was examined by a thermocouple embedded in the mold. As a result, it was found that the material was kept at a high temperature of 470 ° C. or higher during the time t 1 to t 2 = 12 seconds. In this holding process, the load of the press is also P 1 = 600
It fell from ton to P 2 = 500 ton. The decrease in the pressing force indicates that the material softens and the deformation resistance decreases due to the increase in the material temperature.

【0017】次いで、時点t3 =37秒で加圧力P1
600トンに到達するように荷重を再度上昇させ、第2
段階の鍛造を行った。第2鍛造工程後、プレスに加えて
いる負荷を解放し、鍛造製品を金型から取り出した。鍛
造製品の形状を観察したところ、図4(a)及び(b)
に実線で示すように巻き終り2e及び巻き始め2sの何
れにおいても、欠肉部2e'及び欠肉部2s'がみられなか
った。得られたスクロールは、所期目標の肉厚5mm及
び高さ35mmに高精度で一致したラップ2が形成され
ていた。すなわち、保持工程で軟質化した素材が第2鍛
造工程で塑性流動し、欠肉部2e'及び欠肉部2s'に当る
金型キャビティに肉が補給されていることが判る。
Next, at time t 3 = 37 seconds, the pressing force P 1 =
The load is increased again to reach 600 tons and the second
Staged forging was performed. After the second forging step, the load applied to the press was released, and the forged product was taken out of the mold. When the shape of the forged product is observed, FIGS. 4 (a) and 4 (b)
As shown by the solid line, neither the winding end 2e nor the winding start 2s showed the lacked portion 2e 'and the lacked portion 2s'. In the obtained scroll, the wrap 2 was formed with high precision and with the intended thickness of 5 mm and height of 35 mm. That is, it can be seen that the material softened in the holding step plastically flows in the second forging step, and the meat is replenished in the mold cavities hitting the lacking portion 2e 'and the lacking portion 2s'.

【0018】[0018]

【発明の効果】以上に説明したように、本発明において
は、鍛造を2段階に分け、中間に保持工程をおくことに
より、加工熱を利用して素材を昇温軟質化させている。
そのため、変形抵抗が低減した素材に対し第2段階の鍛
造が施され、金型キャビティの隅々まで肉を補給するこ
とができる。したがって、複雑形状であっても、形状特
性に優れた鍛造製品を得ることができる。しかも、中間
熱処理等を必要とすることなく、荷重を加減することだ
けで同じ金型内にセットされている素材を鍛造すること
から、鍛造作業自体も容易なものとなる。また、大きな
荷重を必要としないため、小型のプレスが使用可能にな
ると共に、金型の寿命も長くなる。
As described above, in the present invention, the forging is divided into two stages, and the holding process is provided in the middle, whereby the heat of working is utilized to soften the material by heating.
Therefore, the material with reduced deformation resistance is subjected to the second stage forging, and the meat can be supplied to every corner of the mold cavity. Therefore, it is possible to obtain a forged product having excellent shape characteristics even if the shape is complicated. Moreover, since the material set in the same die is forged only by adjusting the load without the need for intermediate heat treatment or the like, the forging operation itself becomes easy. Further, since a large load is not required, a compact press can be used and the life of the mold is extended.

【図面の簡単な説明】[Brief description of drawings]

【図1】 複雑形状をもつ製品例としてのコンプレッサ
ー用スクロール
Fig. 1 Scroll for compressor as an example of product with complicated shape

【図2】 同スクロールを鍛造で製造するときの問題を
説明する図
FIG. 2 is a diagram illustrating a problem when the scroll is manufactured by forging.

【図3】 本発明に従った加圧力の経時変化を示すグラ
FIG. 3 is a graph showing a change in applied pressure with time according to the present invention.

【図4】 本発明の作用・効果を具体的に表わした図FIG. 4 is a diagram specifically showing the operation and effect of the present invention.

【符号の説明】[Explanation of symbols]

1 フランジ 1a,1b フランジ
の端面 2,2a,2b ラップ 2s ラップの巻き始
め 2e ラップの巻き終り 2s',2e' 欠肉部 3 ボス
1 Flange 1a, 1b End face of flange 2, 2a, 2b Wrap 2s Wrap winding start 2e Wrap winding end 2s ', 2e' Notched portion 3 Boss

Claims (1)

【特許請求の範囲】[Claims] 【請求項1】 歯高H及び歯厚TがH/T≧5の形状を
もつスクロールに対応したキャビティを有する金型にア
ルミニウム合金素材をセットし、該素材の材質,製品の
形状,加工温度等によって定まる所定圧力まで加圧する
ことにより、目標形状のほぼ全体を成形する第1鍛造工
程、そのままのプレス位置で前記素材を保持する保持工
程、及び加圧力が若干低下した後で加圧力を再度上昇さ
せて最終形状に成形する第2鍛造工程を備えていること
を特徴とするアルミニウム合金の鍛造方法。
1. An aluminum alloy material is set in a mold having a cavity corresponding to a scroll having a tooth height H and a tooth thickness T of H / T ≧ 5, and the material of the material, the shape of the product, and the processing temperature. The first forging step of forming almost the entire target shape by pressing to a predetermined pressure determined by the above, the holding step of holding the raw material in the press position as it is, and the pressing force being slightly decreased again. A forging method for an aluminum alloy, characterized by comprising a second forging step of raising to form a final shape.
JP19294292A 1992-06-26 1992-06-26 Forging method for aluminum alloy Pending JPH067877A (en)

Priority Applications (1)

Application Number Priority Date Filing Date Title
JP19294292A JPH067877A (en) 1992-06-26 1992-06-26 Forging method for aluminum alloy

Applications Claiming Priority (1)

Application Number Priority Date Filing Date Title
JP19294292A JPH067877A (en) 1992-06-26 1992-06-26 Forging method for aluminum alloy

Publications (1)

Publication Number Publication Date
JPH067877A true JPH067877A (en) 1994-01-18

Family

ID=16299576

Family Applications (1)

Application Number Title Priority Date Filing Date
JP19294292A Pending JPH067877A (en) 1992-06-26 1992-06-26 Forging method for aluminum alloy

Country Status (1)

Country Link
JP (1) JPH067877A (en)

Cited By (5)

* Cited by examiner, † Cited by third party
Publication number Priority date Publication date Assignee Title
JPH0910884A (en) * 1995-06-22 1997-01-14 Nissan Motor Co Ltd Production of forged product
JP2003112513A (en) * 2001-10-04 2003-04-15 Denso Corp Air conditioner for vehicle
WO2006129608A1 (en) * 2005-06-01 2006-12-07 Honda Motor Co., Ltd. Die reinforcing method and die repairing method
JP2012006066A (en) * 2010-06-28 2012-01-12 Nippon Steel Corp Method for forging workpiece
CN109570417A (en) * 2018-11-23 2019-04-05 哈尔滨工业大学 A kind of accurate forming method of aluminium alloy thin-walled curved surface muscle forging

Cited By (6)

* Cited by examiner, † Cited by third party
Publication number Priority date Publication date Assignee Title
JPH0910884A (en) * 1995-06-22 1997-01-14 Nissan Motor Co Ltd Production of forged product
JP2003112513A (en) * 2001-10-04 2003-04-15 Denso Corp Air conditioner for vehicle
WO2006129608A1 (en) * 2005-06-01 2006-12-07 Honda Motor Co., Ltd. Die reinforcing method and die repairing method
US8337639B2 (en) 2005-06-01 2012-12-25 Honda Motor Co., Ltd. Die reinforcing method and die repairing method
JP2012006066A (en) * 2010-06-28 2012-01-12 Nippon Steel Corp Method for forging workpiece
CN109570417A (en) * 2018-11-23 2019-04-05 哈尔滨工业大学 A kind of accurate forming method of aluminium alloy thin-walled curved surface muscle forging

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