CN109915054A - A kind of fracturing sand buries the Refloatation method of stuck flow controller - Google Patents
A kind of fracturing sand buries the Refloatation method of stuck flow controller Download PDFInfo
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- CN109915054A CN109915054A CN201910239067.3A CN201910239067A CN109915054A CN 109915054 A CN109915054 A CN 109915054A CN 201910239067 A CN201910239067 A CN 201910239067A CN 109915054 A CN109915054 A CN 109915054A
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- flow controller
- fishing
- sand
- tool string
- wire rope
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Abstract
The invention belongs to oil-gas mining technical fields, and the Refloatation method of stuck flow controller is buried more particularly to a kind of fracturing sand.Include the following steps, progress drifting first judges flow controller depth;Then it descends lead stamp tool string to combine, judges fracturing sand situation;Next replacement fishing sand tool string combination carries out fishing sand operation, and until fishing sand is completed, lead stamp is judged as flow controller fishing neck;Finally decentralization fishing socket tool string combination, crawl flow controller constantly above propose jarring, salvage until completing flow controller.To make underground whether belong to fracturing sand burial judge it is simpler accurately, more efficient to the salvaging of fracturing sand, the salvaging for burying stuck flow controller for fracturing sand is more efficient.
Description
Technical field
The invention belongs to oil-gas mining technical fields, and the salvaging side of stuck flow controller is buried more particularly to a kind of fracturing sand
Method.
Background technique
At present in the problem flow controller complex process operation of underground, stuck flow controller is buried for fracturing sand in the prior art
Refloatation method, disclose less, only retrieve, there is disclosure, continuous oil on the 8th Ningxia Young Scientist Forum collected works
Manifold technology refers in salvaging the exploration application on flow controller, encounter gas well shake out flow controller buried by fracturing sand when, can be with
Sediment outflow is carried out in such a way that well head is set a raft going, however this discharging modes are only able to satisfy gas well flow controller reference performance
Under sand discharge, the case where and its emission effect is also unsatisfactory, or Gas well blocking cementing for that fracturing sand, is but
It is unable to satisfy requirement.
Summary of the invention
The present invention provides the Refloatation methods that a kind of fracturing sand buries stuck flow controller.
Specific technical solution is that the fracturing sand buries the Refloatation method of stuck flow controller, is included the following steps, (1) is logical
Well, decentralization drifting tool string combination, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+gauguste cutter complete drifting,
Judge flow controller depth;(2) lead stamp tool string combines under, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+lead
Print, lead stamp judgment result displays have fracturing sand trace;(3) lead stamp tool string combination out, replacement fishing sand tool string combination, steel wire are played
Rope socket+weighted lever+universal joint+bumper jar+bailers carries out fishing sand operation, and until fishing sand is completed, lead stamp is judged as that flow controller is beaten
Fish out neck;(4) combination of decentralization fishing socket tool string, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+fishing socket are grabbed
It takes flow controller constantly above to propose jarring, is salvaged until completing flow controller.
Further, if fishing sand is completed in step (3), but flow controller can not be still grabbed, transfers lead stamp tool
String combination, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+lead stamp, lead stamp judgment result displays have a little throttling
Device center-pole, but there is still gravel traces, transfer the combination of crocodile clip tool string, wire rope socket+rotary joint+weighted lever+universal
Section+bumper jar+crocodile clip removes the cementing fracturing sand in fish head position, again repeatedly step (3).
Further, decentralization fishing socket tool string combination, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+
Fishing socket, grabs flow controller, and upward jarring is unable to complete flow controller unfreezing and above mentions, then cuts fishing socket pin, replace blind hammer
Tool string combination, wire rope socket+weighted lever+universal joint+bumper jar+blind hammer, downward jarring flow controller, until flow controller downlink,
Step (4) are repeated again until flow controller salvages completion.
Further, bumper jar is spring bumper jar.
Whether the present invention completes stuck to underground throttle device to be that fracturing sand buries progress accurate judgement by lead stamp determining method,
Then make the judgement for whether thering is fracturing sand to bury more accurate by the combination of special fishing tool string, the salvaging of fracturing sand
More efficiently;And it is further, judged by lead stamp determining method with the presence or absence of the cementing situation of fracturing sand, and pass through
Tool string combination is significantly more efficient to solve fracturing sand cementing the technical issues of causing flow controller that can not salvage, and covers fracturing sand
Bury the salvaging more convenient and efficient of stuck flow controller.
Specific technical solution
Embodiment 1 is completed flow controller in Soviet Union's 36-11-16H well and is salvaged.Soviet Union's 36-11-16H well construction relevant parameter, such as
Under, well type-diameter;Flow controller model-CQXD-71 to be salvaged;Gas production tree type-standard christmas tree salvages depth 1497m, oil
Pipe specification 3 1/2, casing pressure 3.44MPa.
Pump type bailers is a kind of pump-type tool, routinely lift pump and piston principle;It is set when sand is deposited on underground
Standby top, prevents when being normally carried out of salvaging, and lower bailers clears up fracturing sand.
When work, connector is above put on, piston rod, the piston being attached thereto move upwards together, and steel ball moves upwards at this time,
Sand in well is pumped;Top connection is transferred, steel ball drop is located in an eyelet, and the sand pumped is blocked by steel ball, is retained
In cylinder, extraction reciprocal in this way acts tool until rock sand is filled in cylinder.It is provided by supplier in the market.Such as treasured
The pump type bailers of Ji Jinhui petroleum machinery Co., Ltd production.
On October 18th, 2013 launches successfully: to after 1700 meters, decentralization flow controller to 850 meters of place's chance decks is sealed for drifting,
The flow controller for meeting deck envelope is salvaged afterwards and launches 1 new flow controller again to 1500 meters;On January 23rd, 2018 is caught at 1496 meters
It mentions motionless on flow controller, successively replaces pin three times, because jarring is multiple, pin is disconnected, salvages failure.
On July 12nd, 2018 flow controller in Soviet Union's 36-11-16H well is salvaged using technical solution of the present invention.
9:10 construction team reaches well site, holds pre-shift meeting, does safety education and training, arranges construction site, handles and go into operation
License.
9:40 well head installs lubricator pressure testing.
9:45 starts drifting, tool string combination (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation connects
Head+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 73*230mm gauguste cutter, drifting
It visits to 1497m to flow controller, slowly acts tool string.It is attached between tool and tool using PEC quick coupling.
Flow controller is pounded under 10:20 under blind hammer, tool string combines (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*1000mm weighted lever+Φ 38*300mm universal joint+Φ 38*
The blind hammer of 1560mm bumper jar+Φ 70mm*480mm, pounds deblocking flow controller under 1497 meters, secondary using pounding more than 50 under two weighted levers
Fail to pound flow controller, acts tool string and replace tool.
Fishing socket under 11:10, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation
Connector+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 38*1230mm spring jarring
Device+Φ 70*480mm fishing socket, at the 1497m under grab flow controller, under grab and repeatedly fail to grip with flow controller, act tool string and replace lead
Print.
Lead stamp under 11:55, tool string combination (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation connects
Head+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 71*300mm lead stamp, under slow
It puts tool light pound at 1497 meters and plays out tool string, lead stamp can show flow controller center-pole, and bottom simultaneously has a little sand
Gravel.
12:40, down-pump type bailers, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm
Rotary joint+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 71*2200mm fishes out sand
Cylinder fishes out sand at 1497m, and decentralization, which is slightly tapped downwards to 1497 meters using bumper jar, makes bailers internal piston as most lower
End is pumped to piston upwards generation lower end negative pressure in bailers silt quickly above mentioning tool, and repeated work is three times
It acts tool and checks fishing sand situation, discovery has a little fracturing sand to be pulled out when dismantling bailers lower end, bailers of dismantling.
Fishing socket under 13:35, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation
Connector+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+38*1160mm accelerator+Φ
38*1230mm spring bumper jar+Φ 70*480mm fishing socket, at the 1497m under grab flow controller, successfully catch flow controller, above mention
Tension folds the unlock of the folded spring locking mechanism moment in spring bumper jar to 400Kg, repeats No. more than 30 flow controller deblockings of unlocked step, delays
Slowly above mention, above mention by being hampered when box cupling, each box cupling, which will use, to be hit 4-5 times on folded spring bumper jar and could pass through, above mention to
Flow controller is stuck at 899 meters can not above mention in box cupling, next pound and pound flow controller under the blind hammer of disconnected pin replacement.
Flow controller is pounded under 15:10 under blind hammer, tool string combines (from top to bottom): Φ 38*180mm wire rope socket Φ 38*
280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*1000mm weighted lever+Φ 38*300mm universal joint+Φ 38*
The blind hammer of 1560mm bumper jar+Φ 70mm*480mm, pounds flow controller under 899 meters, is throttled using pounding more than 20 times under two weighted levers
It pounds under device to 990m, acts tool string and replace tool.
Fishing socket under 15:50, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation
Connector+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+38*1160mm accelerator+Φ
38*1230mm spring bumper jar+Φ 70*480mm fishing socket, at the 990m under grab flow controller, successfully catch flow controller, above mention logical
Smoothly benefit is salvaged to well head, and flow controller is salvaged successfully.
17:00 tidies up construction tool, restores construction site, and construction terminates.
A large amount of fracturing sands are arranged at the well flow controller top, cause flow controller that can not grab salvaging, eventually by present techniques
Scheme has smoothly completed salvaging.
Embodiment 2 is completed flow controller in Soviet Union's 36-16-13H2 well and is salvaged.Soviet Union's 36-16-13H2 well construction relevant parameter,
It is as follows, well type-diameter;Flow controller model-RD-71 to be salvaged;Christmas tree model-KQ65/105, gas production tree type-standard gas production
Tree salvages depth 1557m, oil pipe specification 3 1/2, casing pressure 3.44MPa.
The success of RD-71 type flow controller is launched by 23 Pai Bo Lectra October in 2013
18 Pai Bo made every effort to overcome and salvaged flow controller failure October in 2016, can not catch flow controller at 1548 meters, beat lead stamp hair
Existing greasy dirt and center-pole offset.
On July 16th, 2018 flow controller in Soviet Union's 36-16-13H2 well is salvaged using technical solution of the present invention.
8:50 reaches well site, holds pre-shift meeting, does safety education and training, arranges construction site, handles the license that goes into operation.
9:30 shaft mouth anti-blowout pipe pressure testing.
10:00 starts drifting, and tool string combines (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation
Connector+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 72*230mm gauguste cutter leads to
Well is hampered to 1534m, slowly acts tool string.
Lead stamp judges underground situation under 10:50, and tool string combines (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+72*200mm lead
Print is hampered in 1534m and plays lead stamp sample.It acts tool string, there is the trace of fracturing sand in lead stamp.
Lower bailers, tool string combine (from top to bottom) to 12:10 for the first time: Φ 38*180mm wire rope socket+Φ 38*
1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 70*1350mm bailers.Bailed sand amount
1.5kg。
Second of 13:50 lower bailers, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 70*1350mm bailers.Bailed sand amount
1.2kg。
The lower bailers of 15:30 third time, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 70*1350mm bailers.Bailed sand amount
0.2kg。
Lead stamp judges underground situation under 16:50, and tool string combines (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+72*20mm lead
Print is hampered in 1534m and plays lead stamp sample.It acts tool string, still there is the trace of large stretch of fracturing sand in lead stamp.It is preliminary to judge close to fish head
Position fracturing sand is cementing harder.
18:00 terminates to construct, and salvages failure.
On July 17th, 2018, Xianyang are illustrious and influential to second of flow controller fishing of the well
9:40 reaches well site, holds pre-shift meeting, does safety education and training, arranges construction site, the license that goes into operation is handled, to well
Mouth lubricator pressure testing.
Crocodile clip under 10:50, so that the fracturing sand above fish head continues to salvage fracturing sand, tool string group after slightly loosening a bit
It closes (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*
300mm universal joint+Φ 38*1560mm bumper jar+38*400mm crocodile clip acts tool string above fish head after activity repeatedly.
Bailers under 12:50, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*1200mm is aggravated
Universal+Φ 38*1560mm bumper jar+Φ 70*1350mm the bailers of bar+Φ 38*300mm.Bailed sand amount 1.5kg.
14:10 stops construction because raining, and salvages failure.
On August 7th, 2018, Xianyang are illustrious and influential to the well third time flow controller fishing.
9:00 reaches well site, holds pre-shift meeting, does safety education and training, arranges construction site, the license that goes into operation is handled, to well
Mouth lubricator pressure testing.
Lower bailers, tool string combine (from top to bottom) to 9:40 for the first time: Φ 38*180mm wire rope socket+Φ 38*
1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 70*1350mm bailers.Bailed sand amount
0.8kg。
Second of 11:00 lower bailers, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 70*1350mm bailers.Bailed sand amount
0.3kg overhauls bailers.
The lower bailers of 12:20 third time, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 70*1350mm bailers.Bailed sand amount
0.2kg。
Lead stamp judges underground situation under 13:10, and tool string combines (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*
280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 72*200mm
Lead stamp, acts tool string, and lead stamp sample is flow controller fishing neck.
Fishing socket under 14:10, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation
Connector+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 38*480mm' fishing socket,
Under grab repeatedly after successfully arrest flow controller, jarring more than 30 times, fishing socket pin is disconnected, and throttling does not unseal.
15:40 combines (from top to bottom) with flow controller, tool string is pounded under blind hammer: Φ 38*180mm wire rope socket+Φ 38*
280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 38*100mm
Blind hammer, under pound and pound 0.5m under No. more than 60 flow controllers, act tool string.
Fishing socket under 17:00, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation
Connector+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 38*480mm fishing socket, under
Flow controller is successfully arrested after grabbing six or seven times, jarring is multiple, and it is stuck above to mention 20m for flow controller deblocking.Throttle positions 1514m is salvaged
Cylinder pin nail fracture, acts tool string.
18:20 terminates to construct, and salvages failure.
On August 8th, 2018, to No. the 4th flow controller fishing of the well
8:50 reaches well site, holds pre-shift meeting, does safety education and training, arranges construction site, the license that goes into operation is handled, to well
Mouth lubricator pressure testing.
9:30 combines (from top to bottom) with flow controller, tool string is pounded under blind hammer: Φ 38*180mm wire rope socket+Φ 38*
280mm rotary joint+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 38*100mm
Blind hammer, under pound and pound 2m under No. more than 40 flow controllers, act tool string.
Fishing socket under 10:50, tool string combine (from top to bottom): Φ 38*180mm wire rope socket+Φ 38*280mm rotation
Connector+Φ 38*1200mm weighted lever+Φ 38*300mm universal joint+Φ 38*1560mm bumper jar+Φ 38*480mm fishing socket,
Flow controller is successfully arrested at 1514m, activity is lifted from the top and puted down repeatedly, slowly above mentions, and meets card at each hoop.It throttles after 3.5h
Device is salvaged successfully.
14:30 terminates to construct, and restores construction site.
Whether the present invention completes stuck to underground throttle device to be that fracturing sand buries progress accurate judgement by lead stamp determining method,
Then make the judgement for whether thering is fracturing sand to bury more accurate by the combination of special fishing tool string, the salvaging of fracturing sand
More efficiently;And it is further, judged by lead stamp determining method with the presence or absence of the cementing situation of fracturing sand, and pass through
Tool string combination is significantly more efficient to solve fracturing sand cementing the technical issues of causing flow controller that can not salvage, and covers fracturing sand
Bury the salvaging more convenient and efficient of stuck flow controller.
Claims (4)
1. the Refloatation method that a kind of fracturing sand buries stuck flow controller, it is characterised in that: include the following steps, (1) drifting, transfer
The combination of drifting tool string, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+gauguste cutter complete drifting, judge to throttle
Device depth;(2) lead stamp tool string combines under, and wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+lead stamp, lead stamp is sentenced
It is disconnected to have fracturing sand trace as the result is shown;(3) replacement fishing sand tool string combination, wire rope socket+weighted lever+universal joint+bumper jar+fishing
Sand cylinder carries out fishing sand operation, and until fishing sand is completed, lead stamp is judged as flow controller fishing neck;(4) fishing socket tool string group is transferred
It closing, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+fishing socket, crawl flow controller constantly above proposes jarring, until
Flow controller is completed to salvage.
2. the Refloatation method that fracturing sand according to claim 1 buries stuck flow controller, it is characterised in that: in step (3)
In if fishing sand is completed, but can not still grab flow controller, decentralization lead stamp tool string combination, wire rope socket+rotary joint+plus
Weight bar+universal joint+bumper jar+lead stamp, lead stamp judgment result displays have a little flow controller center-pole, but there is still gravel trace,
The combination of crocodile clip tool string is transferred, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+crocodile clip removes fish head portion
The cementing fracturing sand in position, again repeatedly step (3).
3. the Refloatation method that fracturing sand according to claim 1 buries stuck flow controller, it is characterised in that: decentralization fishing socket
Tool string combination, wire rope socket+rotary joint+weighted lever+universal joint+bumper jar+fishing socket grab flow controller, upward jarring
It is unable to complete flow controller unfreezing and above mentions, then cut fishing socket pin, replace blind hammer tool string and combine, wire rope socket+weighted lever+
Universal joint+bumper jar+blind hammer, downward jarring flow controller, until flow controller downlink, repeatedly step (4) is beaten until flow controller again
Fishing is completed.
4. the Refloatation method that fracturing sand according to any one of claims 1 to 3 buries stuck flow controller, it is characterised in that:
Bumper jar is folded spring bumper jar.
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CN115162992A (en) * | 2022-06-30 | 2022-10-11 | 中石化石油工程技术服务有限公司 | Small-diameter pipe column cutting and fishing integrated fishing device and method |
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Application publication date: 20190621 |